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34-013-20500

Well Details

Well ID: 34-013-20500
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Country: United States
State: Ohio
County: Belmont
Municipality: York Township
Operator Name: CALDWELL RANDY D
Well Pad ID:
Farm/Lease Name: CALDWELL
License Status: Domestic Well
License Date: 1987-06-22
Spud Date: 1987-06-26
Spud Drilling Contractor: SWANK-ULLMAN
Final Drill Date: 1987-07-01
Well Total Depth: 2210.00 ft
Configuration: Vertical
Latitude: 39.870000
Longitude: -80.900000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1987-06-22 Issued Date 6/22/87 Expired Date 6/21/88 Acres 0020000 Tool Type RTA Proposed Formation WEIR Proposed Depth 02210 Proposed Drill Depth 02210
Original Spud 1987-06-26 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM KEROGEN RESOURCES #3054 TO OWNER ON 9/15/2016 CM.
Completed 1987-07-01 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM KEROGEN RESOURCES #3054 TO OWNER ON 9/15/2016 CM.
Reached Total Depth 1987-07-01 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM KEROGEN RESOURCES #3054 TO OWNER ON 9/15/2016 CM.
CO 1987-07-15 3054 KEROGEN RESOURCES GeoDate 6/22/87
Completion Report Received 1988-05-18 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM KEROGEN RESOURCES #3054 TO OWNER ON 9/15/2016 CM.
Construction Permit Expires 1988-06-21 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM KEROGEN RESOURCES #3054 TO OWNER ON 9/15/2016 CM.
Change of Owner 2016-09-15 Operator changed from 3054, KEROGEN RESOURCES to 9766, CALDWELL RANDY D
Record Last Modified 2017-02-15 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM KEROGEN RESOURCES #3054 TO OWNER ON 9/15/2016 CM.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 2068 2133 37
2070 2140 0
1997-06-29 2070 2140 0
2068 2133 37
2068 2133 37

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 200 Mscf 0
H2O 0 93500 Gal 90200 FRAC: H2O,SAND,N2
ACID 15 750 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 PETRO DRILLING CORP 3188.00 304.00 120
1988 PETRO DRILLING CORP 8838.00 220.00 365
1989 KEROGEN RESOURCES 6863.00 77.00 356
1990 KEROGEN RESOURCES 4299.00 0.00 364
1991 KEROGEN RESOURCES 2481.00 0.00 365
1992 KEROGEN RESOURCES 3591.00 17.00 365
1993 KEROGEN RESOURCES 2879.00 0.00 365
1994 KEROGEN RESOURCES 2826.00 0.00 365
1995 KEROGEN RESOURCES 2407.00 0.00 365
1996 KEROGEN RESOURCES 2194.00 35.00 365
1997 KEROGEN RESOURCES 2005.00 0.00 365
1998 KEROGEN RESOURCES 2538.00 0.00 365
1999 KEROGEN RESOURCES 2019.00 0.00 305
2000 KEROGEN RESOURCES 453.00 26.00 65
2001 KEROGEN RESOURCES 1985.00 0.00 275
2002 KEROGEN RESOURCES 1603.00 0.00 215
2003 KEROGEN RESOURCES 1559.00 0.00 245
2004 KEROGEN RESOURCES 1738.00 24.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 PETRO DRILLING CORP Brine 173 120
1988 PETRO DRILLING CORP Brine 306 365
1989 KEROGEN RESOURCES Brine 131 356
1990 KEROGEN RESOURCES Brine 46 364
1991 KEROGEN RESOURCES Brine 33 365
1992 KEROGEN RESOURCES Brine 40 365
1993 KEROGEN RESOURCES Brine 34 365
1994 KEROGEN RESOURCES Brine 33 365
1995 KEROGEN RESOURCES Brine 33 365
1996 KEROGEN RESOURCES Brine 31 365
1997 KEROGEN RESOURCES Brine 30 365
1998 KEROGEN RESOURCES Brine 35 365
1999 KEROGEN RESOURCES Brine 31 305
2000 KEROGEN RESOURCES Brine 12 65
2001 KEROGEN RESOURCES Brine 19 275
2002 KEROGEN RESOURCES Brine 17 215
2003 KEROGEN RESOURCES Brine 16 245
2004 KEROGEN RESOURCES Brine 18 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1244867856 2016-3-15 0:00: PW No Violations 2.50
-1265115366 2004-12-15 0:00 PW No Violations
-1904957798 2005-8-15 8:44: PW No Violations
-345892268 2006-2-3 0:00:0 PW No Violations
-951207865 2013-1-15 0:00: PW No Violations 0.50
0010615985 2008-03-18 Production Wells No Violations PRODUCING WELL
005604i162 2002-04-25 Production Wells No Violations
0155727006 2012-01-24 Production Wells Violations Noted On the day of my inspection the well was equipped with a pumping unit. The tank battery contained one 110 barrel oil storage tank, one 25 barrel brine storage tank, and a mechanical separator. There was a oil stain present from a stuffing box leak that measured approximately 2 foot by 2 foot. This well is capable of production, however production has not been submitted since 2004. UPDATE: 01/09/2014 Status of well has not changed.
0345892268 2006-02-03 Production Wells No Violations WELL IS IN PRODUCTION.
0407863285 2008-10-16 Production Wells No Violations WELL APPEARS TO BE IDLE. ALL PRODUCING EQUIPMENT ON WELLSITE, BUT DOES NOT APPEAR TO HAVE BEEN IN PRODUCTION.
0640492044 2003-12-11 Production Wells No Violations STATUS CHECK, DOMESTIC GAS.
0649510613 2016-04-21 Production Wells No Violations On this day I was accompanied by Brent Bear. This inspection was a follow up to a previous release that occurred at this site. This site still needs addressed. Soil with oil contamination is still present inside and outside of the dike area. The operator shall address these issues through more remediation efforts.
0858176006 2004-07-28 Production Wells No Violations STATUS CHECK, WELL APPEARS TO BE IN PRODUCTION
0866783188 2008-07-30 Production Wells No Violations NO PRODUCTION REPORTS SINCE YR. 2004. SHOULD BE BROUGHT TO MCCORMACS ATTENTION.
0900684156 2016-10-24 Production Wells No Violations This well remains in the same state as last inspection. It has been transferred to the landowner for domestic use. The area tank battery area still needs addressed so that the Compliance Notice may be resolved. I will contact the landowner concerning this issue.
0951207865 2013-01-15 Production Wells No Violations I spoke with the owner and operator of this well Kim Cecil. He informed me that the well was being sold to Rice Energy and paperwork was being finalized. He also stated that his production records would be up to date very soon. All violations will be resolved at that time.
10615985 2008-3-18 0:00: PW No Violations
1244867856 2016-03-15 Production Wells No Violations On this day I visited the site in response to a call received concerning a spill that had occurred. Upon reviewing the affected area I determined that further remediation was necessary. The owner was contacted. (03/14/2016) Site will be monitored until proper remediation is complete. See complaint #5275.
1265115366 2004-12-15 Production Wells No Violations WELL IS STILL IN PRODUCN. WITH CHARLIE ENSIGNER.
1310424232 2006-04-19 Production Wells No Violations STATUS CHECK. NO PRODUCTION REPORTS FILED SINCE 2004.
1458005864 2016-03-14 Production Wells Violations Noted On this day I received notification by phone at 18:02 hours from a local contractor Troy Harmon with Harmons Well Service that He had a water truck in-root to the well site to recover fluid that had leaked from the production tank, Mr. Harmon indicated the landowner Randy Caldwell contacted Him after He was unable to reach the producer Kim Cecil. I arrived on location and witnessed Harmons Well Service water truck remove a total of 6 barrels of oil from inside the production tank dike area, all fluid was also removed from the 100 barrel production tank that appeared to have leaked. A area of approximately 2x 100was also impacted outside the dike area. Also noted was on this day at 20:27 pm I contacted the registered well owner Kerogen Resources and spoke Kim Cecil at (740-787-2989) and informed Him that the tank had leaked and the issue needed addressed, Mr. Cecil indicated the lease had been severed and the landowner was the owner of the well, at that point I indicated to Mr. Cecil that He was the registered owner with the Division and He agreed to address the issue. Instructions are as follows. Immediately stabilize , remove and remediate the oil & brine impacted areas inside the dike.
1458217620 2016-03-17 Production Wells No Violations Follow up inspection to complaint 5275 regarding the production tank associated with the said well leaking fluid onto the owners property. A violation was issued identified as inspection # 1458005864 issued on 03/14/2016. Upon inspection on this day it was observed that the affected area of the spill has had straw applied to it, the landowner Randy Caldwell reported He applied the straw to the area. The area affected by the product outside the dike area was measured at a recorded distance of 157 at the longest affected point and 2 at the widest point. The product outside the dike appears to be at a minimal amount present however there is product inside the dike under the straw that needs recovered. Also noted was the following was found at the well head- 4.5 production casing and 1.5 production tubing equipped with a production tree and pumping rods with the well set up to be produced by the means of a pumping unit. The commercial production valves were found in the closed position and the valve on the domestic supply side was found in the open position supporting the statement from the landowner that He is using the well for domestic purposes. The commercial gas sales meter was found to have no current sales chart present.
1458670592 2016-03-22 Production Wells No Violations Follow up inspection to complaint 5275 regarding the production tank associated with the said well leaking fluid onto the owners property. A violation was issued identified as inspection # 1458005864 issued on 03/14/2016. Upon inspection of the area affected by the production fluid leaking from the 100 barrel production tank it was observed that no attempt has been made by the producer to recover the remaining product that is inside or outside the earthen dike area.
1470661373 2016-08-02 Exempt Well Pre Transfer No Violations An inspection was conducted as a follow up for the bonding and surety section. The landowner has stated via phone that this well is currently producing domestic gas. The well is equipped in the same manner as the previous inspection. Contact was made to the current owner, Kim Cecil, via voicemail on 08/05/2016. Kim was instructed to finish the restoration of this site from the previous oil release. A follow up inspection will be conducted once Mr. Cecil has finished the restoration. Photos were taken on the day of the inspection.
1484335221 2017-01-13 Production Wells No Violations My inspection revealed that the well appeared to be equipped properly to be considered capable of providing domestic gas to the landowner. The tank battery that the landowner has previously stated would be removed was still erect. The tank battery was in satisfactory condition and the previous Compliance Notice is eligible to be closed at this time.
155727006 2012-1-24 0:00: PW No Violations 0.50
1602771764 2017-04-28 Production Wells No Violations This well has been changed to a domestic ownership. Work has been performed, by the domestic owner, to alleviate the environmental concerns. The previous compliance notice has been resolved.
1725950159 2004-04-08 Production Wells No Violations STATUS CHECK
1756174944 2007-01-31 Production Wells No Violations STATUS CHECK
1904957798 2005-08-15 Production Wells No Violations Status check
2056678543 2005-11-21 Production Wells No Violations WELL IN PRODUCTION. PRODUCTION REPORTS CAUGHT UP TO 2004.
407863285 2008-10-16 0:00 PW No Violations
5604i162 2002-4-25 0:00: PW No Violations
640492044 2003-12-11 0:00 PW No Violations
649510613 2016-4-21 0:00: PW No Violations 1.00
858176006 2004-7-28 0:00: PW No Violations
866783188 2008-7-30 0:00: PW No Violations
900684156 2016-10-24 0:00 PW No Violations 1.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0155727006 US-OH-115183 2017-05-26 NONE_ Nonproduction; well shall be plugged or placed in temporary inactive status
0155727006 US-OH-115184 2017-05-26 NONEC Statement of annual production not filed
1458005864 US-OH-113267 2016-03-17 Well operation causing pollution and contamination
1458005864 US-OH-113268 2016-03-17 No SPCC dike/or failure to keep dike free of water or oil

For data sources see[9]

References