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34-013-20350

Well Details

Well ID: 34-013-20350
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Country: United States
State: Ohio
County: Belmont
Municipality: Somerset Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: DOUDNA
License Status: Final Restoration
License Date: 2016-02-29
Spud Date: 1981-03-16
Spud Drilling Contractor:
Final Drill Date: 1981-03-21
Well Total Depth: 3750.00 ft
Configuration: Vertical
Latitude: 39.940000
Longitude: -81.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-09-30 1902 DUCK CREEK ENERGY INC GeoDate 9/30/80
Oil and Gas 1980-09-30 Issued Date 9/30/80 Expired Date Acres 0020000 Tool Type RTA Proposed Formation OHIO SHALE Proposed Depth 03750 Proposed Drill Depth 03750
Original Spud 1981-03-16
Completed 1981-03-21
Reached Total Depth 1981-03-21
Completion Report Received 1981-04-27
CO 1986-06-09 1902 DUCK CREEK ENERGY INC GeoDate 6/9/86
Unknown 1986-06-09 Issued Date 6/9/86 Expired Date 6/9/87 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
CO 1997-03-04 24 ROCANVILLE CORPORATION GeoDate 6/9/86
Change of Owner 2003-06-24 Operator changed from 24, ROCANVILLE CORPORATION to 4540, PEOPLES PETROLEUM CORP.
Change of Owner 2005-10-05 Operator changed from 4540, PEOPLES PETROLEUM CORP. to 1634, NORTHWOOD ENERGY CORP
APP 2015-12-21 Proposed Formations:OHIO SHALE, Issued Date:12/21/2015, Expired Date:12/20/2017 12:00:00 PM, Drilling unit acres:129, Proposed Well Type:OG, Proposed Well Class:
APP 2016-02-29 Proposed Formations:OHIO SHALE, Issued Date:2/29/2016, Expired Date:2/28/2018 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-04-05
Record Last Modified 2017-02-10
Construction Permit Expires 2018-02-28

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 OBERLE JAMES LTD 215.00 69.00 0
2003 PEOPLES PETROLEUM CORP. 0.00 0.00 0
2004 WHITED ROGER 0.00 0.00 365
2005 NORTHWOOD ENERGY CORP 0.00 0.00 0
2006 NORTHWOOD ENERGY CORP 0.00 0.00 0
2007 NORTHWOOD ENERGY CORP 0.00 60.00 365
2008 NORTHWOOD ENERGY CORP 0.00 25.00 365
2009 NORTHWOOD ENERGY CORP 258.00 0.00 365
2010 NORTHWOOD ENERGY CORP 61.00 0.00 365
2011 NORTHWOOD ENERGY CORP 64.00 0.00 0
2012 NORTHWOOD ENERGY CORP 78.00 40.00 366
2013 NORTHWOOD ENERGY CORP 29.00 0.00 365
2014 NORTHWOOD ENERGY CORP 24.00 0.00 365
2015 NORTHWOOD ENERGY CORP 0.00 5.00 365
2016 NORTHWOOD ENERGY CORP 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 OBERLE JAMES LTD Brine 0 0
2003 PEOPLES PETROLEUM CORP. Brine 0 0
2004 PEOPLES PETROLEUM CORP. Brine 0 0
2005 NORTHWOOD ENERGY CORP Brine 0 0
2006 NORTHWOOD ENERGY CORP Brine 0 0
2007 NORTHWOOD ENERGY CORP Brine 80 365
2008 NORTHWOOD ENERGY CORP Brine 100 365
2009 NORTHWOOD ENERGY CORP Brine 33 365
2010 NORTHWOOD ENERGY CORP Brine 53 365
2011 NORTHWOOD ENERGY CORP Brine 70
2012 NORTHWOOD ENERGY CORP Brine 63 366
2013 NORTHWOOD ENERGY CORP Brine 62 365
2014 NORTHWOOD ENERGY CORP Brine 0 365
2015 NORTHWOOD ENERGY CORP Brine 73 365
2016 NORTHWOOD ENERGY CORP Brine 193 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1157452944 2015-7-10 0:00: PW No Violations
-1182495915 2015-4-3 0:00:0 PW No Violations 0.50
-1250246777 2016-10-11 0:00 FR No Violations 1.00
-1341011457 2016-3-22 0:00: PB No Violations 5.00
-1574259396 2015-9-25 0:00: PW No Violations 0.50
-1648698382 2015-4-24 0:00: PW No Violations 0.50
-1683917453 2012-12-5 0:00: PW No Violations 0.50
-1878362740 2016-4-4 0:00:0 PB No Violations 5.00
-2089425707 2016-3-15 0:00: PB No Violations 5.50
-425909267 2013-4-4 0:00:0 PW No Violations 0.50
-745498766 2016-3-16 0:00: PB No Violations 7.00
-890439715 2016-3-29 0:00: PB No Violations 3.50
0005604i55 2002-01-29 Production Wells No Violations
0425909267 2013-04-04 Production Wells No Violations On the day of my inspection the well was equipped with a pumping unit and was capable of production. The tank battery contents included: one 100 bbl oil storage tank and one mechanical separator. No violations were noted.
0446988120 2014-09-24 Production Wells No Violations Onsite with Inspector Andrew Corder. Site contents include 100 bbl oil tank, a mechanical seperator, and a pumping unit on the wellhead. Well has all the required equipment to produce.
0563640861 2014-09-24 Production Wells No Violations On the day of my inspection the well had a pumping unit and all equipment to be capable of production. The tank battery contents included a 100 bbl oil storage tank and a separator. No violations noted.
0577237614 2016-03-17 Plug / Plug Back No Violations On site along with county inspector to discuss options concerning plugging of said well, Davis Well Service currently is washing 2.875 tubing over 1.5 tubing it was stuck in hole and they are currently at 3200 and they are having trouble with power swivel and they hope to be back in operation tomorrow.
0626917790 2016-03-28 Plug / Plug Back No Violations I attemped to contact Glen Davis and Earl Barnes with no success. I visited the site to get updated on the progress of this plugging operation and there was no activity taking place.
0685957219 2015-02-11 Production Wells Violations Noted I received an email from Gene Chini of the Orphan Well Program. He had received a call from Greg Martin alleging that the well does not produce enough products to meet the requirements of the Ohio Revised Code. The well is equipped with the necessary equipment to be capable of production. The tank battery contents include: one 100 bbl oil storage tank and one mechanical separator. This well has produced domestic gas in the past but the landowner claims it is not currently supplying gas. RBDMS records of production demonstrate that this well does not produce enough oil, gas, or combination thereof to meet the State regulation. Company shall plug this well within 180 days.
0745498766 2016-03-16 Plug / Plug Back No Violations On this day the operator had tripped back to bottom with the 2.875 tubing. They have lost ground and tagged up above the point they had washed to the previous day. This indicates the possibility of a hole in the 4.5 casing up hole casing debris to fall onto the backside of the 1.5 tubing. Washing operators continued today with about 8 of progress. Operator will continue washing operations tomorrow.
0890439715 2016-03-29 Plug / Plug Back No Violations On this day the operator tripped 2.875 tubing back into the hole with an overshot tool. Once on the 1.5 tubing the operator pulled to try and recover the tubing. After several attempts the 1.5 parted. The operator pulled 3 joints and tripping operations will continue tomorrow.
0913814174 2016-03-11 Plug / Plug Back No Violations On this day the company was attempting to wash 2.875 tubing down to free the 1.5 tubing so that it may be recovered prior to plugging operations commencing.
0934355334 2016-03-08 Plug / Plug Back No Violations
0989530891 2016-03-17 Plug / Plug Back No Violations On this day the operator had tripped back to bottom with the 2.875 tubing. They tagged up at approximately the same depth they had reached in the previous day. Washing operations had success today and they were making progress. Toward the end of the day the swivel had broken down. The operator is working to remedy the mechanical issues. Once they the swivel is fixed the washing operations will resume.
1060555939 2016-03-23 Plug / Plug Back No Violations On site with county inspector to discuss upcoming plugging operation.
1126724469 2005-09-14 Production Wells No Violations C/O TO ROGER WHITED. NO PRODUCTION FILED SINCE 2003. CAPABLE OF PRODUCTION.
1157452944 2015-07-10 Production Wells No Violations Email sent to Bill Arnholt. This is a reminder of the Compliance Notice that I issued. This issue needs to be addressed. I will not grant an extension on this Notice.
1182495915 2015-04-03 Production Wells No Violations An email was sent to Bill Arnholt of Northwood Energy. The email was to address questions that Bill had asked. I informed him that he needed to address the issue of insufficient production and he questioned if the oil in the tank was shipped and met State requirements would the Compliance be cleared. I told him to submit the documentation to me and I would clear the notice. I also reminded him this action needed to take place by 08/11/2015
1250246777 2016-10-11 Final Restoration No Violations This site has been restored and has passed final restoration.
1341011457 2016-03-22 Plug / Plug Back No Violations The operator has repaired the swivel and washing operators have commenced again.
1452608765 2016-03-10 Plug / Plug Back No Violations
1457953271 2016-03-09 Plug / Plug Back No Violations On this day the Davis Wells service rig was moved onto location. The planned operations were to pull the rods from the well and determine how to proceed with plugging operations. Rod retrieval operations were unsuccessful and it was determined that a stripping job would have to be performed.
1458588170 2016-03-21 Plug / Plug Back No Violations On this day the operator was attempting to fix the swivel unit. It was determined that bearings were needed and the unit was taken to the shop for repairs.
1459257536 2016-03-29 Plug / Plug Back No Violations The operator had to get new slips because the ones they had were non operational. Fishing operations for the 1.5 tubing are to start back up today.
1459775311 2016-03-31 Plug / Plug Back No Violations On this day the operator attemped to drill and wash around the 1.5 tubing to free it from the hole. Operations were not successful and it was determined that the bottom hole plug will be set from 3150 to 2400.
1459950999 2016-04-01 Plug / Plug Back No Violations On this day the cementing process of the plugging operations commenced. Cemenco was on site and set the bottom hole plug from 3150-2305 using Class A cement. The cement was set through the 2.875 tubing. Cement procedures utilized 65 sacks of Class A cement and 13.4 barrels of water to displace the cement plug to the proper depth.
1574259396 2015-09-25 Production Wells No Violations On the day of my inspection the well was equipped with a pumping unit and appeared to have all equipment to be considered capable of production. The valves coming from the well head were in the off position. The tank battery contents include: one 100 bbl oil storage tank and one mechanical separator. Due to the proper equipment and reported production this well will not be required to be plugged. The Compliance Notice for this well is now resolved. See inspection 685957219 for resolved notice.
1576277387 2015-05-22 Production Wells No Violations Email sent to Bill Arnholt. Just another reminder of this Compliance Notice. This notice must be addressed before 08/11/2015. No extension will be granted.
1584558493 2016-04-05 Plug / Plug Back No Violations

--550--

1628245077 2015-08-11 Production Wells No Violations On the day of my inspection the well was equipped to be capable of production. The valve off of the well head leading to the tank battery appeared to be in the closed position. The valves in the tank battery leading to the sales and separation tank appeared to be closed as well. The chart on the metering system appeared to represent no activity. I have made attempts to contact the operator to remedy this compliance notice for the last 6 months with no progress. Photos were taken on the day of the inspection. The landowner, Greg Martin, was present and he inquired about further actions.
1648698382 2015-04-24 Production Wells No Violations Email sent to Bill Arnholt of Northwood Energy. Just another reminder of this Compliance Notice.
1683917453 2012-12-05 Production Wells No Violations On the day of my inspection the well was equipped with a pumping unit and was capable of production. The tank battery contents included: one 100 bbl oil storage tank and one mechanical separator. No violations were noted.
1731149004 2016-03-30 Plug / Plug Back No Violations On this day the 2.875 tubing was tripped from the hole to see if any 1.5 tubing was retrieved. The 1.5 tubing was tallied and the operator was able to recover 1.5 down to 3150. Planned operations are to try and wash down over the 1.5 tubing again to free it from the hole.
1878362740 2016-04-04 Plug / Plug Back No Violations

-

2089425707 2016-03-15 Plug / Plug Back No Violations On this day the operator was attempting to use a tooth bit and fluid to wash down around the 1.5 tubing to free it from the hole. The operator is having little success in washing the debris out from the hole around the 1.5 tubing. The operator will continue to wash in attempt to free the tubing.
446988120 2014-9-24 0:00: PW No Violations 1.00
5604i55 2002-1-29 0:00: PW No Violations
563640861 2014-9-24 0:00: PW No Violations 1.00
577237614 2016-3-17 0:00: PB No Violations
626917790 2016-3-28 0:00: PB No Violations 1.50
685957219 2015-2-11 0:00: PW No Violations 0.50
913814174 2016-3-11 0:00: PB No Violations 2.00
934355334 2016-3-8 0:00:0 PB No Violations 0.50
989530891 2016-3-17 0:00: PB No Violations 8.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0685957219 US-OH-127759 2015-11-10 Well shall be plugged

For data sources see[7]

References