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Well ID: 34-009-23500 | Loading map...
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Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: Bern Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: S LEWIS | |
License Status: Final Restoration | |
License Date: 2014-11-25 | |
Spud Date: 1992-11-05 | |
Spud Drilling Contractor: WARREN DRLG | |
Final Drill Date: 1992-11-14 | |
Well Total Depth: 5089.00 ft | |
Configuration: Vertical | |
Latitude: 39.440000 | |
Longitude: -81.860000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1992-10-15 | 198 VIKING RESOURCES CORP GeoDate 10/15/92 |
Oil and Gas | 1992-10-15 | Issued Date 10/15/92 Expired Date 10/15/93 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05089 Proposed Drill Depth 05089 |
Original Spud | 1992-11-05 | |
Completed | 1992-11-14 | |
Reached Total Depth | 1992-11-14 | |
Completion Report Received | 1992-12-22 | |
Change of Owner | 1998-07-01 | Operator changed from 198, VIKING RESOURCES CORP to 3793, ENERGY SEARCH INC |
Change of Owner | 2008-02-26 | Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2014-11-25 | Proposed Formations:CLINTON, Issued Date:11/25/2014, Expired Date:11/24/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-06-09 | |
Construction Permit Expires | 2016-11-24 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4880 | 4912 | 0 |
4880 | 4912 | 0 | |
2006-09-11 | 4892 | 4989 | 35 |
4892 | 4989 | 35 | |
4880 | 4912 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 82000 Gal | 80000 | FRAC W/82M GAL H20 & 800 SX SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | VIKING RESOURCES LLC | 25497.00 | 55.00 | 365 |
1994 | VIKING RESOURCES LLC | 17253.00 | 57.00 | 365 |
1995 | VIKING RESOURCES LLC | 6861.00 | 0.00 | 0 |
1996 | VIKING RESOURCES LLC | 4108.00 | 19.00 | 0 |
1997 | VIKING RESOURCES LLC | 4076.00 | 0.00 | 0 |
1998 | VIKING RESOURCES LLC | 1166.00 | 0.00 | 365 |
1999 | ENERGY SEARCH INC | 2599.00 | 0.00 | 365 |
2000 | ENERGY SEARCH INC | 1687.00 | 0.00 | 365 |
2001 | ENERGY SEARCH INC | 1061.00 | 0.00 | 365 |
2002 | ENERGY SEARCH INC | 898.00 | 0.00 | 365 |
2003 | ENERGY SEARCH INC | 681.00 | 0.00 | 365 |
2004 | ENERGY SEARCH INC | 513.00 | 0.00 | 365 |
2005 | ENERGY SEARCH INC | 875.00 | 0.00 | 365 |
2006 | ENERGY SEARCH INC | 1155.00 | 0.00 | 365 |
2007 | ENERGY SEARCH INC | 148.00 | 0.00 | 59 |
2008 | EXCO - NORTH COAST ENERGY INC | 0.00 | 33.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 94 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | VIKING RESOURCES LLC | Brine | 1244 | 365 |
1994 | VIKING RESOURCES LLC | Brine | 171 | 365 |
1995 | VIKING RESOURCES LLC | Brine | 443 | 0 |
1996 | VIKING RESOURCES LLC | Brine | 183 | 0 |
1997 | VIKING RESOURCES LLC | Brine | 197 | |
1998 | VIKING RESOURCES LLC | Brine | 154 | 365 |
1999 | ENERGY SEARCH INC | Brine | 185 | 365 |
2000 | ENERGY SEARCH INC | Brine | 147 | 365 |
2001 | ENERGY SEARCH INC | Brine | 159 | 365 |
2002 | ENERGY SEARCH INC | Brine | 16 | 365 |
2003 | ENERGY SEARCH INC | Brine | 121 | 365 |
2004 | ENERGY SEARCH INC | Brine | 59 | 365 |
2005 | ENERGY SEARCH INC | Brine | 0 | 365 |
2006 | ENERGY SEARCH INC | Brine | 0 | 365 |
2007 | ENERGY SEARCH INC | Brine | 0 | 59 |
2008 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 0 |
2010 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2011 | ENERVEST OPERATING LLC | Brine | 0 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2013 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2015 | ENERVEST OPERATING LLC | Brine | 0 | 94 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1057741759 | 2015-6-8 0:00:0 | PB | No Violations | 5.80 |
-2072754907 | 2015-8-10 0:00: | FR | No Violations | 0.80 |
0009191632 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 3/24/94 INSPECTOR DAN GOINS DATE 03/2419/94 DATA FROM OLD VAX INFO | |
0043504859 | 2015-06-05 | Plug / Plug Back | No Violations | Witnessed plugging operations. The bottom hole plug was set from 4868-4468 through tubing using 35 sacks of Class A cement. |
0288475950 | 2015-06-09 | Plug / Plug Back | No Violations | Witnessed plugging operations. The Berea plug that was set yesterday afternoon was tagged this morning at 1823 feet. The fluid level is staying consistent around 400 feet. Circulation established and another Berea plug was placed through tubing from 1737-1537 with 60 sacks of Class A cement, the bottom of the surface casing plug was ran with the berea plug from 1537-1300 with 65 sacks of Class A cement, and the surface plug was set from 170 to surface with 50 sacks of Class A cement. |
1057741759 | 2015-06-08 | Plug / Plug Back | No Violations | Witnessed plugging operations. Telegraph was located and the 4 1/2 casing was ripped at 2927, one joint was pulled to be sure the pipe was free and the pump truck began to establish circulation. While the truck was pumping the pressures increased and the pipe locked up. The wellhead was unpacked and fluid was moved using the pump truck. Two more joints were pulled and circulation was again established. A 300 foot Class A cement plug was placed from 2775-2475 and oil was circulated from the hole and then fell back. The 4 1/2 casing was pulled up to 1746 and a 200 foot plug was placed across the Berea sandstone. Again oil circulated from the hole and then fell back as soon as water came on. The well will be shut in and the plug will be tagged tomorrow. |
1433526580 | 2015-06-04 | Plug / Plug Back | No Violations | Pulling tubing. A half round steel tank will be used for circulation instead of a pit. |
1775351607 | 2014-09-04 | Production Wells | Violations Noted | Well equipped with a plunger lift system. The valves on the well were all closed. Company has reported zero as production since 2010. Well shall be plugged. |
2013267735 | 2012-03-27 | Production Wells | No Violations | The well is equipped with a plunger lift system. The dike had 2 mechanical separators, one 100 barrel production tank, one 60 barrel production tank, and a 1100 gallon production tank with 600 gallons of fluid in it. The plastic production tank was not physically connected to any of the other tanks. A 200 barrel production tank was located outside the dike. No violations at time of inspection. |
2072754907 | 2015-08-10 | Final Restoration | No Violations | Final restoration check. The wellsite has been passed as of 6/22/15, I visited the tank battery and the tanks associated with the Lewis #2 have been removed. Restoration passed. |
2132268115 | 2015-06-22 | Plug / Plug Back | No Violations | The well site has been graded and has vegetative cover returning, the lease road has a few bare sites. No equipment at well site and a half round steel 100 bbl tank was used for circulation so there are no pits to close. I meet Tim McConnaughey at the tank battery and we discussed removing the tanks to meet the Final Restoration requirements. |
288475950 | 2015-6-9 0:00:0 | PB | No Violations | 3.70 |
43504859 | 2015-6-5 0:00:0 | PB | No Violations | 3.30 |
9191632 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1775351607 | US-OH-117685 | 2015-07-29 | Well shall be plugged |
For data sources see[9]