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34-007-22539

Well Details

Well ID: 34-007-22539
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Country: United States
State: Ohio
County: Ashtabula
Municipality: Andover Township
Operator Name: EXCO - NORTH COAST ENERGY INC
Well Pad ID:
Farm/Lease Name: COE
License Status: Final Restoration
License Date: 1988-08-15
Spud Date: 1984-12-01
Spud Drilling Contractor: SHERMAN DRLG
Final Drill Date: 1984-12-04
Well Total Depth: 3999.00 ft
Configuration: Vertical
Latitude: 41.620000
Longitude: -80.550000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1983-12-15 1388 NORTH COAST ENERGY INC GeoDate 12/15/83
Oil and Gas 1983-12-15 Issued Date 12/15/83 Expired Date 6/12/84 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1984-10-31 1388 NORTH COAST ENERGY INC GeoDate 10/31/84
Oil and Gas 1984-10-31 Issued Date 10/31/84 Expired Date 4/29/85 Acres 0020000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 03999 Proposed Drill Depth 03999
Original Spud 1984-12-01 FIELD INSPECTED BY INSPECTOR KOHL ON 6/14/16 AND WELL NOT FOUND. NO PLUGGING REPORT FOR THIS WELL - USED INSPECTION DATE FOR PLUGGING DATE. FINAL RESTORATION APPROVED.
Completed 1984-12-04 FIELD INSPECTED BY INSPECTOR KOHL ON 6/14/16 AND WELL NOT FOUND. NO PLUGGING REPORT FOR THIS WELL - USED INSPECTION DATE FOR PLUGGING DATE. FINAL RESTORATION APPROVED.
Reached Total Depth 1984-12-04 FIELD INSPECTED BY INSPECTOR KOHL ON 6/14/16 AND WELL NOT FOUND. NO PLUGGING REPORT FOR THIS WELL - USED INSPECTION DATE FOR PLUGGING DATE. FINAL RESTORATION APPROVED.
Completion Report Received 1985-01-14 FIELD INSPECTED BY INSPECTOR KOHL ON 6/14/16 AND WELL NOT FOUND. NO PLUGGING REPORT FOR THIS WELL - USED INSPECTION DATE FOR PLUGGING DATE. FINAL RESTORATION APPROVED.
CO 1988-08-15 1388 NORTH COAST ENERGY INC GeoDate 8/15/88
Unknown 1988-08-15 Issued Date 8/15/88 Expired Date 8/15/89 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Construction Permit Expires 1989-08-15 FIELD INSPECTED BY INSPECTOR KOHL ON 6/14/16 AND WELL NOT FOUND. NO PLUGGING REPORT FOR THIS WELL - USED INSPECTION DATE FOR PLUGGING DATE. FINAL RESTORATION APPROVED.
Plugged/Abandoned 2016-06-14 FIELD INSPECTED BY INSPECTOR KOHL ON 6/14/16 AND WELL NOT FOUND. NO PLUGGING REPORT FOR THIS WELL - USED INSPECTION DATE FOR PLUGGING DATE. FINAL RESTORATION APPROVED.
Record Last Modified 2019-06-05 FIELD INSPECTED BY INSPECTOR KOHL ON 6/14/16 AND WELL NOT FOUND. NO PLUGGING REPORT FOR THIS WELL - USED INSPECTION DATE FOR PLUGGING DATE. FINAL RESTORATION APPROVED.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3875 3927 12
3875 3927 12
3875 3927 12

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 94670 Gal 50000 FRAC:WATER,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 EXCO - NORTH COAST ENERGY INC 3546.00 69.00 0
1986 EXCO - NORTH COAST ENERGY INC 4655.00 67.00 365
1987 EXCO - NORTH COAST ENERGY INC 2262.00 0.00 365
1988 EXCO - NORTH COAST ENERGY INC 1019.00 0.00 160

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 EXCO - NORTH COAST ENERGY INC Brine 385 0
1986 EXCO - NORTH COAST ENERGY INC Brine 740 365
1987 EXCO - NORTH COAST ENERGY INC Brine 198 365
1988 EXCO - NORTH COAST ENERGY INC Brine 445 160

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1054201582 2016-6-14 0:00: FR No Violations
1054201582 2016-06-14 Final Restoration No Violations My inspection of this well found no sign of the tank battery or the well on the surface. There was a plugging permit issued for this well on 8-15-1988 but there was no record of plugging the well. I approved the final restoration.

For data sources see[9]

References