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34-007-22412

Well Details

Well ID: 34-007-22412
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Country: United States
State: Ohio
County: Ashtabula
Municipality: Denmark Township
Operator Name: BOCOR HOLDINGS, LLC
Well Pad ID:
Farm/Lease Name: HENTON
License Status: Plugged and Abandoned
License Date: 1988-02-01
Spud Date: 1983-12-04
Spud Drilling Contractor: IPSCO
Final Drill Date: 1983-12-05
Well Total Depth: 3556.00 ft
Configuration: Vertical
Latitude: 41.720000
Longitude: -80.690000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1983-11-07 935 HUTCHESON RH/BoCOR PROD GeoDate 11/7/83
Oil and Gas 1983-11-07 Issued Date 11/8/83 Expired Date 5/5/84 Acres 0042710 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 03556 Proposed Drill Depth 03556
Completed 1983-12-04 WELL CARD DATA

PI 11/12/83

Original Spud 1983-12-04 WELL CARD DATA

PI 11/12/83

Reached Total Depth 1983-12-05 WELL CARD DATA

PI 11/12/83

Completion Report Received 1984-07-31 WELL CARD DATA

PI 11/12/83

CO 1988-02-01 935 HUTCHESON RH/BoCOR PROD GeoDate 2/1/88
Unknown 1988-02-01 Issued Date 2/1/88 Expired Date Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Construction Permit Expires 1989-01-31 WELL CARD DATA

PI 11/12/83

Plugging Plan Approved 1998-02-12 WELL CARD DATA

PI 11/12/83

Record Last Modified 2016-05-17 WELL CARD DATA

PI 11/12/83

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3359 3401 12
3359 3401 12
3359 3401 12

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 0 0
H2O 0 1500 Bbl 50000 FRAC;WATER,SAND,&N2
N2 0 0 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 CAREY RESOURCES INC 1891.00 107.00 365
1986 CAREY RESOURCES INC 0.00 65.00 365
1987 CAREY RESOURCES INC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 CAREY RESOURCES INC Brine 133 365
1986 CAREY RESOURCES INC Brine 0 365
1987 CAREY RESOURCES INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-44017096 2013-8-5 0:00:0 PB No Violations
0044017096 2013-08-05 Plug / Plug Back No Violations Complainant, Katherine . I met with Kevin Hutcheson with the company , We then procceeded to search for the well . After a very extensive search we could not locate the well location . We discussed the options for locating the well . Kevin decided to get equipment to excavate the well to determine if the well was plugged . Case is pending the excavation of the well .
1393871856 2014-09-10 Final Restoration No Violations Complaint#4369 , Katherine . I met with Kevin Hutcheson on site . He excavated the well and found there was a cap welded onto the surface casing below the surface . There was no indication the well was leaking . This well has been plugged . The final restoration has been completed . NO VIOLATIONS . THIS COMPLAINT HAS BEEN RESOLVED .

For data sources see[9]

References