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| Well ID: 34-005-61871 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Ashland | |
| Municipality: Perry Township | |
| Operator Name: FAWN RESOURCES LLC | |
| Well Pad ID: | |
| Farm/Lease Name: DONELSON | |
| License Status: Producing | |
| License Date: | |
| Spud Date: 1950-10-23 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1950-12-05 | |
| Well Total Depth: 2765.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.840000 | |
| Longitude: -82.200000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Reached Total Depth | 1950-12-05 | HAROLD MORAVY INSPECTED WELL ON 7/31/2008. THIS IDLE, BEREA WELL HAS 7" CASING ABOVE GROUND. |
| Change of Owner | 2014-08-12 | Operator changed from 8182, MOHICAN RIVER ENERGY HOLDINGS to 9315, FAWN RESOURCES LLC |
| Record Last Modified | 2014-08-13 | HAROLD MORAVY INSPECTED WELL ON 7/31/2008. THIS IDLE, BEREA WELL HAS 7" CASING ABOVE GROUND. |
For data sources see[2]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2011 | MOHICAN RIVER ENERGY HOLDINGS | 0.00 | 0.00 | 0 |
| 2012 | MOHICAN RIVER ENERGY HOLDINGS | 0.00 | 0.00 | 365 |
| 2013 | MOHICAN RIVER ENERGY HOLDINGS | 0.00 | 0.00 | 181 |
| 2014 | FAWN RESOURCES LLC | 0.00 | 0.00 | 0 |
| 2015 | FAWN RESOURCES LLC | 0.00 | 0.00 | 0 |
| 2016 | FAWN RESOURCES LLC | 0.00 | 0.00 | 0 |
| 2017 | FAWN RESOURCES LLC | 0.00 | 0.00 | 0 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2011 | MOHICAN RIVER ENERGY HOLDINGS | Brine | 0 | |
| 2012 | MOHICAN RIVER ENERGY HOLDINGS | Brine | 0 | 365 |
| 2013 | MOHICAN RIVER ENERGY HOLDINGS | Brine | 0 | 181 |
| 2014 | FAWN RESOURCES LLC | Brine | 0 | 0 |
| 2015 | FAWN RESOURCES LLC | Brine | 0 | 0 |
| 2016 | FAWN RESOURCES LLC | Brine | 0 | 0 |
| 2017 | FAWN RESOURCES LLC | Brine | 0 | 0 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| 1489768074 | 2017-03-17 | Production Wells | No Violations | There is open surface casing in the well. The casing is full of water which is currently frozen. There is an old wellhead on the casing which is cracked and broken. About a third of the wellhead is broken off and laying next to the well. There is no road to the location and the well is idle. The operator will need to service this well to return it to production. Fawn Resources acquired this well from Mohican River Energy as part of a group of wells and they are working to place wells in production. They have not started on this property yet. |
For data sources see[7]