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34-005-23912

Well Details

Well ID: 34-005-23912
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Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: GORTNER R & P
License Status: Active Injection
License Date: 1990-10-17
Spud Date: 1990-12-11
Spud Drilling Contractor: M&G OIL CO.
Final Drill Date: 1991-01-02
Well Total Depth: 744.00 ft
Configuration: Vertical
Latitude: 40.890000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Enhanced Recovery 1990-10-17 Issued Date 10/17/90 Expired Date 10/17/91 Acres 0123750 Tool Type RTA Proposed Formation BEREA Proposed Depth 00744 Proposed Drill Depth 00744
Original Spud 1990-12-11
Completed 1991-01-02
Reached Total Depth 1991-01-02
CO 1991-04-25 133 QUAKER STATE OIL REF CORP GeoDate 10/17/90
First Injection 1991-04-25
Completion Report Received 1991-05-21
Construction Permit Expires 1991-10-17
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 10/17/90
Annulus Pressure Monitoring Approved 1997-11-12
Last Compliance Report 1999-10-25
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-22 545 685 0
545 685 0
545 685 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 140 Lbs 0 SHOT FROM 545-685 W/140# 80% GEL

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC 0.00 133.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1055902461 2018-8-15 0:00: ER No Violations
-1077280315 2016-7-8 0:00:0 ER No Violations
-1188077037 2014-7-17 0:00: ER No Violations
-126767066 2020-4-22 0:00: ER No Violations
-1390466476 2010-11-26 0:00 ER No Violations 1.00
-1411364174 2018-4-27 0:00: ER No Violations
-1506079115 2008-12-3 0:00: ER No Violations 0.50
-1540109869 2009-10-7 0:00: ER No Violations 1.00
-1595607623 2012-9-20 0:00: ER No Violations
-1845431823 2011-7-12 0:00: ER No Violations
-1866487196 2011-11-17 0:00 ER No Violations
-1908185210 2012-9-20 0:00: ER No Violations
-195035549 2019-1-14 0:00: ER No Violations
-2014399866 2012-11-27 0:00 ER No Violations
-2103364744 2013-3-4 0:00:0 ER No Violations
-326096593 2016-10-19 0:00 ER No Violations
-400762163 2013-5-22 0:00: ER No Violations
-427956859 2012-3-7 0:00:0 ER No Violations
-501968141 2019-8-5 0:00:0 ER No Violations
-60741912 2003-11-13 0:00 ER No Violations
-848631508 2004-4-22 0:00: ER No Violations
-873059010 2015-9-28 0:00: ER No Violations
-905072548 2015-3-31 0:00: ER No Violations
-975285113 2018-10-12 0:00 ER No Violations
0023452942 2013-08-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0060741912 2003-11-13 Enhanced Recovery Project No Violations
0099280767 2018-01-30 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The annulus test port valve was frozen due to the cold weather during inspection.
0208808425 2016-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in poor condition.
0288148305 2014-10-28 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0289234770 2014-05-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0294516871 2017-04-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0316913045 2012-06-04 Enhanced Recovery Project No Violations Inspect Well.
0326096593 2016-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The nipple on the well head is in poor condition.
0340272863 2015-05-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0357908738 2016-01-07 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0400762163 2013-05-22 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0409040896 2008-03-25 Enhanced Recovery Project Violations Noted Annulus and injection pressure test. Annular side is 0 psi. Pump up to 200 psi and test.
0413688065 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0427956859 2012-03-07 Enhanced Recovery Project No Violations Inspect Well.
0456791485 2006-12-14 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0657629187 2015-10-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The operator replaced the well head fittings. The wall is in compliance.
0657739243 2018-02-28 Enhanced Recovery Project No Violations Re-Inspect well for integrity. Well head fittings were frozen during previous inspection.
0821952595 2011-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0848631508 2004-04-22 Enhanced Recovery Project No Violations Injection pressure test.
0873059010 2015-09-28 Enhanced Recovery Project No Violations Inspect well at request of operator. The injection tubing tee is currently leaking and has not been repaired.
0880402816 2013-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0905072548 2015-03-31 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0975285113 2018-10-12 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0995966938 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
1055902461 2018-08-15 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1077280315 2016-07-08 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in fair condition.
1145885871 2006-04-24 Enhanced Recovery Project No Violations Injection and annular pressure test.
1174480501 2017-10-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1188077037 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head has a slight leak.
1193646240 2005-05-19 Enhanced Recovery Project No Violations Injection well test. Update GPS readings.
1201505474 2019-10-24 0:00 ER No Violations
1208350814 2008-04-16 Enhanced Recovery Project No Violations Annulus and injection pressure test. Pressured annular side to 200 psi for 15 minutes and had 0 psi decline. Advised Len Rex to resume injection. NOV in compliance. Sun, 40 degrees.
1240491890 2009-04-23 Enhanced Recovery Project No Violations Injection and and annulus pressure test.
1390466476 2010-11-26 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1411364174 2018-04-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1431088125 2007-10-12 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1506079115 2008-12-03 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Annular side is 0 psi. injection is 320 psi. Needs identification.
1519161049 2007-03-08 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1540109869 2009-10-07 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1572329819 2006-01-25 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1595607623 2012-09-20 Enhanced Recovery Project No Violations Inspect Well. Site ok.
1654401970 2017-01-30 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1738623202 2017-07-31 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1838080931 2015-08-31 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The injection line fitting were leaking.
1845431823 2011-07-12 Enhanced Recovery Project No Violations inspect well.
1866487196 2011-11-17 Enhanced Recovery Project No Violations Inspect well. ID miss marked.
1898237736 2016-11-07 Enhanced Recovery Project No Violations Operator performed repairs on well and replaced fittings that were in poor condition.
1908185210 2012-09-20 Enhanced Recovery Project No Violations Inspect Well. Site ok.
1945641741 2008-12-10 Enhanced Recovery Project No Violations Mini test on annulus. Pressured up to 200 psi and 0 psi decline in 15 minutes.
2014399866 2012-11-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
208808425 2016-4-19 0:00: ER No Violations
2103364744 2013-03-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
23452942 2013-8-29 0:00: ER No Violations
288148305 2014-10-28 0:00 ER No Violations
289234770 2014-5-27 0:00: ER No Violations
294516871 2017-4-13 0:00: ER No Violations
316913045 2012-6-4 0:00:0 ER No Violations
340272863 2015-5-13 0:00: ER No Violations
357908738 2016-1-7 0:00:0 ER No Violations
409040896 2008-3-25 0:00: ER No Violations 1.00
413688065 2014-3-17 0:00: ER No Violations
456791485 2006-12-14 0:00 ER No Violations 0.50
473914630 2020-1-30 0:00: ER No Violations
657629187 2015-10-6 0:00: ER No Violations
657739243 2018-2-28 0:00: ER No Violations
770172662 2020-7-14 0:00: ER No Violations
821952595 2011-4-13 0:00: ER No Violations 0.50
880402816 2013-10-29 0:00 ER No Violations
910876158 2019-4-22 0:00: ER No Violations
99280767 2018-1-30 0:00: ER No Violations
995966938 2004-11-18 0:00 ER No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0409040896 US-OH-124336 2008-03-25 Failure to conduct or pass mech. integrity test
1506079115 US-OH-114199 2008-12-03 Failure to conduct or pass mech. integrity test
1838080931 US-OH-118354 2016-07-26 9-5-09(A)(3) Violation of injection tubing/fitting requirements

For data sources see[9]

References