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34-005-23075

Well Details

Well ID: 34-005-23075
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Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: GORTNER ROBERT & PAULINE
License Status: Active Injection
License Date: 1974-08-21
Spud Date: 1974-11-18
Spud Drilling Contractor:
Final Drill Date: 1974-11-25
Well Total Depth: 640.00 ft
Configuration: Vertical
Latitude: 40.900000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 133 QUAKER STATE OIL REF CORP
Unknown 1802-01-01 Issued Date 8/7/74 Expired Date Acres Tool Type Proposed Formation Proposed Depth Proposed Drill Depth
Original Spud 1974-11-18 DRILLED BY KLAEGER AND BLODGETT KB=1020.5
Completed 1974-11-25 DRILLED BY KLAEGER AND BLODGETT KB=1020.5
Reached Total Depth 1974-11-25 DRILLED BY KLAEGER AND BLODGETT KB=1020.5
Construction Permit Expires 1975-08-07 DRILLED BY KLAEGER AND BLODGETT KB=1020.5
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate
Annulus Pressure Monitoring Approved 1996-10-08 DRILLED BY KLAEGER AND BLODGETT KB=1020.5
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Last Compliance Report 2012-04-13 DRILLED BY KLAEGER AND BLODGETT KB=1020.5
Record Last Modified 2017-02-15 DRILLED BY KLAEGER AND BLODGETT KB=1020.5

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-22 564 618 0
2006-09-11 565 616 0
564 618 0
565 616 0
564 618 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 77 Qts 0 76.5=VOLUME
NITR 0 75 Qts 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC 0.00 133.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1001716355 2016-10-19 0:00 ER No Violations
-1003288294 2011-11-17 0:00 ER No Violations
-1406224678 2011-4-13 0:00: ER No Violations 1.00
-145256152 2016-1-7 0:00:0 ER No Violations
-1539476116 2007-10-12 0:00 ER No Violations 0.50
-1560067233 2014-3-17 0:00: ER No Violations
-172045265 2014-10-28 0:00 ER No Violations
-1792373287 2003-11-13 0:00 ER No Violations
-1792940232 2006-4-25 0:00: ER No Violations 0.50
-184600042 2013-10-29 0:00 ER No Violations
-1937351124 2006-12-14 0:00 ER No Violations 1.00
-1986937947 2008-3-25 0:00: ER No Violations 1.00
-201936363 2017-1-30 0:00: ER No Violations
-2034670375 2020-4-22 0:00: ER No Violations
-2124295071 2013-9-5 0:00:0 ER No Violations 5.00
-239285881 2016-4-19 0:00: ER No Violations
-267983412 2012-11-27 0:00 ER No Violations
-490812675 2014-3-17 0:00: ER No Violations
-86254518 2018-8-15 0:00: ER No Violations
-918102419 2019-1-14 0:00: ER No Violations
-956338696 2014-5-27 0:00: ER No Violations
-97645544 2009-10-7 0:00: ER No Violations 0.50
0050048915 2012-06-04 Enhanced Recovery Project No Violations Inspect Well.
0079794575 2015-08-31 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0086254518 2018-08-15 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0097645544 2009-10-07 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0103178199 2012-09-20 Enhanced Recovery Project No Violations Inspect Well. Site ok.
0145256152 2016-01-07 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Injection valve nipple was partially froze due to cold weather. Well head was thawed out and retested.
0172045265 2014-10-28 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0184600042 2013-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0199479668 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
0201936363 2017-01-30 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0239285881 2016-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0255057548 2007-04-03 Enhanced Recovery Project No Violations Blew down pressure on annulus and pumped up to 260 psi. 0% decline after 15 minutes. NOV in compliance.
0267983412 2012-11-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0295336333 2010-04-05 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0320672643 2017-07-31 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0417727030 2018-01-30 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Inspect well for integrity and pressure.
0440944468 2016-07-08 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0485248423 2015-03-31 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0490812675 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The valve for the injection line and annulus was frozen during previous days inspection. Re-test annulus and injection line on well. Gauge malfunctioned during testing of injection line.
0497397013 2018-04-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head tubing is in poor condition.
0515021579 2009-04-23 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0539597773 2015-10-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in fair condition. The operator was notified there is a drip from the shut off valve stem. The operator subsequently repaired the well valve.
0546384184 2007-03-08 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Pressures are equalized. Reset 1 packer and pressure test. 3-30-07 retested annulus and pressures are equal. Shut in well and repair packer.
0911958274 2006-01-25 Enhanced Recovery Project Violations Noted Injection pressure and annulus pressure are equalized. Reset packer and test.
0956338696 2014-05-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0960832685 2015-05-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1001716355 2016-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The identification need to be updated. Collect brine sample TSB114 from wellhead for chemical analysis.
1003288294 2011-11-17 Enhanced Recovery Project No Violations Well shut in. Has not been serviced. No ID tag.
1023598692 2017-04-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
103178199 2012-9-20 0:00: ER No Violations
1116513659 2005-05-19 Enhanced Recovery Project Violations Noted Injection well is idle. Injection tubing valve is closed. Unable to test at this time. Well needs serviced. Update GPS readings.
1119875527 2005-06-23 Enhanced Recovery Project Violations Noted Well is back on injection. Tested injection pressure at 355psi and annulus pressure at 370 psi. NOV in compliance. Hot, 90 degrees.
1142441761 2006-03-15 Enhanced Recovery Project Violations Noted Re-tested annulus and injection pressures. Nov in compliance. Sun, 35 degrees.
1175257702 2007-03-30 Enhanced Recovery Project No Violations Pulled tension on 1 packer and retested. Pressures equalized at 360 psi. Shut well in untill packer is repaired. Sun, 35 degrees
1211098370 2011-07-12 Enhanced Recovery Project No Violations Inspect well. Well equalized. Shut in well.
1295450796 2011-02-01 Enhanced Recovery Project No Violations Injection and annulus pressure test. Replaced packer. Pumped annular side to 405 psi and 20 psi decline in 15 minutes.
1391327245 2020-7-14 0:00: ER No Violations
1406224678 2011-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1443179982 2013-03-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1470602568 2004-04-22 Enhanced Recovery Project No Violations Injection pressure test. Annular and tubing pressure are equalized. Advised Len Rex to repressure annular space and re-test. Send results to Tom Tomastik.
1539476116 2007-10-12 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1560067233 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The injection and annulus valves were frozen during inspection.
1563337924 2008-12-03 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1582313315 2020-1-31 0:00: ER No Violations
1583858817 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1602349253 2010-11-26 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Pressures are equal at 340 psi. Reset packer and test.
1792373287 2003-11-13 Enhanced Recovery Project No Violations
1792940232 2006-04-25 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1806412133 2019-10-24 0:00 ER No Violations
1910963809 2013-08-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Annulus has equalized with the injector. Well shut in for service.
1937037306 2019-8-5 0:00:0 ER No Violations
1937351124 2006-12-14 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1944304889 2012-02-01 Enhanced Recovery Project No Violations inspect well. Conduct 15 minute test on well and pass.
1985197690 2017-10-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1986937947 2008-03-25 Enhanced Recovery Project No Violations Annulus and injection pressure test.
199479668 2004-11-18 0:00 ER No Violations
2077854820 2018-10-12 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2113061003 2013-05-22 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2124295071 2013-09-05 Enhanced Recovery Project No Violations Requested by the operator to witness installation and pressure test of a new packer in the well. The packer passed pressure test with a 2.9% loss in 15 minutes.
217319697 2019-4-22 0:00: ER No Violations
255057548 2007-4-3 0:00:0 ER No Violations 1.00
295336333 2010-4-5 0:00:0 ER No Violations 0.50
295940409 2020-1-30 0:00: ER No Violations
320672643 2017-7-31 0:00: ER No Violations
417727030 2018-1-30 0:00: ER No Violations
440944468 2016-7-8 0:00:0 ER No Violations
485248423 2015-3-31 0:00: ER No Violations
497397013 2018-4-27 0:00: ER No Violations
50048915 2012-6-4 0:00:0 ER No Violations
515021579 2009-4-23 0:00: ER No Violations 0.50
539597773 2015-10-27 0:00 ER No Violations
546384184 2007-3-8 0:00:0 ER No Violations 1.00
79794575 2015-8-31 0:00: ER No Violations
911958274 2006-1-25 0:00: ER No Violations 0.50
960832685 2015-5-13 0:00: ER No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0546384184 US-OH-126008 2007-03-08 Failure to conduct or pass mech. integrity test
0911958274 US-OH-130415 2006-01-26 Mechanical failure/contamination
1116513659 US-OH-102929 2005-05-19 Well incapable of inj./production
1119875527 US-OH-103043 2005-05-19 Well incapable of inj./production
1142441761 US-OH-103618 2006-01-26 Mechanical failure/contamination
1602349253 US-OH-115715 2010-11-26 Failure to conduct or pass mech. integrity test

For data sources see[9]

References