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34-005-23066

Well Details

Well ID: 34-005-23066
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Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: MANN GLADYS C
License Status: Active Injection
License Date: 1975-04-11
Spud Date: 1975-04-16
Spud Drilling Contractor: SHORTS DRLG
Final Drill Date: 1975-05-02
Well Total Depth: 720.00 ft
Configuration: Vertical
Latitude: 40.890000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1975-04-16 RE-ISSUE & SEC. RECOV. 4-16-75
CO 1975-04-21 133 QUAKER STATE OIL REF CORP GeoDate 4/21/75
Enhanced Recovery 1975-04-21 Issued Date 4/21/75 Expired Date Acres 0000000 Tool Type RTAF Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000
Completed 1975-05-02 RE-ISSUE & SEC. RECOV. 4-16-75
Reached Total Depth 1975-05-02 RE-ISSUE & SEC. RECOV. 4-16-75
Annulus Pressure Monitoring Approved 1994-09-21 RE-ISSUE & SEC. RECOV. 4-16-75
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 4/21/75
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Last Compliance Report 2003-08-11 RE-ISSUE & SEC. RECOV. 4-16-75
Change of Owner 2009-02-04 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Record Last Modified 2017-02-15 RE-ISSUE & SEC. RECOV. 4-16-75

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-22 600 668 0
600 668 0
600 668 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 102 Qts 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC 0.00 13.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1031105108 2015-5-21 0:00: ER No Violations
-1041141469 2011-7-12 0:00: ER No Violations
-1054169670 2019-4-18 0:00: ER No Violations
-1069527216 2007-3-30 0:00: ER No Violations 0.50
-1216707566 2013-8-29 0:00: ER No Violations
-1334367035 2013-5-22 0:00: ER No Violations
-1361616018 2009-10-7 0:00: ER No Violations 0.50
-1566499520 2020-5-13 0:00: ER No Violations
-1705465076 2012-2-27 0:00: ER No Violations
-1743871280 2016-5-9 0:00:0 ER No Violations
-1803895427 2019-11-18 0:00 ER No Violations
-1921762814 2008-3-25 0:00: ER No Violations 1.00
-2031215637 2010-11-27 0:00 ER No Violations 0.50
-2107294959 2016-7-11 0:00: ER No Violations
-372943447 2004-4-22 0:00: ER No Violations
-481841461 2016-1-7 0:00:0 ER No Violations
-492495910 2017-4-27 0:00: ER No Violations
-538301848 2017-10-19 0:00 ER No Violations
-566621851 2004-11-18 0:00 ER No Violations
-579453604 2020-2-24 0:00: ER No Violations
-617103789 2012-6-4 0:00:0 ER No Violations
-674437916 2014-7-17 0:00: ER No Violations
-734942749 2018-10-2 0:00: ER No Violations
-770595211 2006-4-24 0:00: ER No Violations 0.50
-793250628 2014-3-18 0:00: ER No Violations
-973291797 2018-1-4 0:00:0 ER No Violations
0006696153 2012-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0149616241 2013-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0214649012 2013-03-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The initial pressure on annulus was similar to line pressure. Annulus was pressured up to 400 psi and a 15 minute mini pressure test conducted. The final pressure was 400 psi. Well passes test.
0313025122 2014-05-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0352558729 2015-08-31 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The annulus and the injection tubing have equalized. Pressure testing of well head annulus is required.
0372943447 2004-04-22 Enhanced Recovery Project No Violations Injection pressure test. Annular and tubing pressures are equalized. Advised Len rex to repressure annular space and test. Report results to Tom Tomastik.
0481841461 2016-01-07 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0492495910 2017-04-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0538301848 2017-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The operator conducted a monthly pressure test that was witnessed. The annulus had zero pressure loss over fifteen minutes.
0566621851 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
0617103789 2012-06-04 Enhanced Recovery Project No Violations Inspect Well.
0625908752 2015-11-12 Work Over Reconditioning No Violations The well is constructed with 2 3/8 inch tubing at a depth of 590 feet cemented to the surface. The well is open hole to the total depth of 720 feet. The J hook pin was missing on the packer causing the failure. The packer was replaced. Two feet of the top most joint of PVC lined tubing was cut off and then re-threaded. Total of 18 joints of 25 foot sections of PVC lined one Inch tubing and one 23 foot joint of PVC lined tubing was run in the hole with a parmaco style packer set in compression. Approximately 300 gallon of fresh water were pumped through the tubing and circulated to the surface prior to setting the packer. The packer was set and the annulus was pressured up to 390 psi. The pressure was monitored for 15 minutes with zero pressure loss. The well passes the Mechanical Integrity Test. The well head was reconstructed with new parts and put into production.
0630334402 2017-07-14 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The operator discovered a leak with the flexible flow line. The line was dug up and replaced. The well is in compliance.
0651547493 2015-11-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The injection tubing and annulus have equalized. Notified operator, the service rig was subsequently mobilized to well to replace the packer and top joint. Passed Mechanical integrity test on 11/12/2015.
0674437916 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head has a slight leak.
0722519662 2012-09-11 Enhanced Recovery Project No Violations Inspect Well. Site ok.
0729700632 2011-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0734942749 2018-10-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0770595211 2006-04-24 Enhanced Recovery Project No Violations Injection and annular pressure test.
0788906684 2008-12-10 Enhanced Recovery Project No Violations Mini test on annulus. Pressured up to 400 psi and 0 psi decline in 15 minutes.
0793250628 2014-03-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0806968416 2003-08-07 Enhanced Recovery Project No Violations
0973291797 2018-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0996438880 2018-05-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Upon inspection the annulus valve was in very poor condition. The operator replaced the valve and pressured the annulus. The pressure was monitored for 15 minutes with less than 3 percent pressure loss. The well is in compliance.
1031105108 2015-05-21 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The annulus inspection test valve is rusted shut.
1041141469 2011-07-12 Enhanced Recovery Project No Violations inspect well.
1069527216 2007-03-30 Enhanced Recovery Project Violations Noted Annulus and injection pressure test. Annular side is reading 0 psi and injection pressure is 350 psi. Pressure up on annular side to 200 psi and report.
1072400491 2017-01-09 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1116375683 2005-05-17 Enhanced Recovery Project No Violations Injection well test. GPS location and update to RBDMS.
1118565035 2018-08-20 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1120402922 2015-03-31 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Pressure was equalized, well was temporarily shut in. The annulus was pressure tested at 387 PSI with no pressure loss over 15 minutes. Test passed and well was put back into production.
1130729312 2007-10-12 Enhanced Recovery Project No Violations Injection and annulus pressure test. No box around well.
1133454819 2005-12-01 Enhanced Recovery Project Violations Noted Injection and annulus pressures are equalized at 340psi.
1138223262 2006-01-25 Enhanced Recovery Project Violations Noted Packer has been set and pressures are ann. 340 & inj. 350. Snow, 27 degrees.
1166188995 2006-12-15 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1177085956 2007-04-20 Enhanced Recovery Project No Violations Pressure test. Annular side held at 310 psi for 15 minutes with no decline. Injection pressure is 330 psi. NOV in compliance.
1216707566 2013-08-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1266381658 2020-1-28 0:00: ER No Violations
1270558102 2010-04-06 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1286382173 2010-10-06 Enhanced Recovery Project No Violations Installing a separator at injection well head. PSI at 350.
1334367035 2013-05-22 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head injector line valve is seeping.
1361616018 2009-10-07 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1478704206 2016-11-07 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
149616241 2013-10-29 0:00 ER No Violations
1556778093 2015-09-23 Enhanced Recovery Project No Violations Operator conducted pressure test on well. The well was pressure tested for 15 minutes. The pressure loss was less than 1 percent. Well is incompliance. Compliance notice of 8/31/2015 can be resolved.
1671661143 2014-10-28 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1705465076 2012-02-27 Enhanced Recovery Project No Violations inspect well.
1743871280 2016-05-09 Enhanced Recovery Project No Violations Follow up inspection from April 25, 2016. The operator has replaced the fitting that were in poor condition.
1893125547 2008-12-03 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Pressures are equal at 320 psi.
1921762814 2008-03-25 Enhanced Recovery Project No Violations Annulus and injection pressure test.
1958601843 2011-10-17 Enhanced Recovery Project No Violations Inspect well.
2031215637 2010-11-27 Enhanced Recovery Project No Violations Injection and annulus pressure test.
2107294959 2016-07-11 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head fittings have been repaired recently.
2139217621 2016-04-25 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The Injection line nipple is in poor condition.
214649012 2013-3-4 0:00:0 ER No Violations
313025122 2014-5-6 0:00:0 ER No Violations
352106306 2019-1-14 0:00: ER No Violations
352558729 2015-8-31 0:00: ER No Violations
625908752 2015-11-12 0:00 WR No Violations
630334402 2017-7-14 0:00: ER No Violations
651547493 2015-11-2 0:00: ER No Violations
6696153 2012-12-4 0:00: ER No Violations
722519662 2012-9-11 0:00: ER No Violations
729700632 2011-4-13 0:00: ER No Violations 0.50
788906684 2008-12-10 0:00 ER No Violations 0.50
806968416 2003-8-7 0:00:0 ER No Violations
963087416 2019-7-24 0:00: ER No Violations
996438880 2018-5-2 0:00:0 ER No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0352558729 US-OH-123704 2015-10-07 Failure to conduct or pass mech. integrity test
1031105108 US-OH-100504 2015-07-17 Failure to monitor annulus pressure
1069527216 US-OH-101437 2007-03-30 Failure to conduct or pass mech. integrity test
1133454819 US-OH-103391 2005-12-01 Mechanical failure/contamination
1138223262 US-OH-103503 2005-12-01 Mechanical failure/contamination
1893125547 US-OH-119016 2008-12-03 Failure to conduct or pass mech. integrity test

For data sources see[9]

References