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34-005-22347

Well Details

Well ID: 34-005-22347
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Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: HASTINGS H & G
License Status: Active Injection
License Date: 1976-02-05
Spud Date: 1976-07-13
Spud Drilling Contractor: SHORTS DRLG
Final Drill Date: 1976-07-29
Well Total Depth: 687.00 ft
Configuration: Vertical
Latitude: 40.900000
Longitude: -82.140000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1965-02-16 RE-ISSUE 4-23-75, R.I. & SEC. RECOV. 2-11-76 START & STOP DATES & IP. OIL IN NSR.
CO 1976-02-05 133 QUAKER STATE OIL REF CORP GeoDate 2/5/76
Oil and Gas 1976-02-05 Issued Date 2/5/76 Expired Date Acres 0081750 Tool Type CT Proposed Formation BEDFORD Proposed Depth 00000 Proposed Drill Depth 00000
Completed 1976-07-29 RE-ISSUE 4-23-75, R.I. & SEC. RECOV. 2-11-76 START & STOP DATES & IP. OIL IN NSR.
Reached Total Depth 1976-07-29 RE-ISSUE 4-23-75, R.I. & SEC. RECOV. 2-11-76 START & STOP DATES & IP. OIL IN NSR.
Completion Report Received 1977-06-22 RE-ISSUE 4-23-75, R.I. & SEC. RECOV. 2-11-76 START & STOP DATES & IP. OIL IN NSR.
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 2/5/76
Annulus Pressure Monitoring Approved 1999-02-04 RE-ISSUE 4-23-75, R.I. & SEC. RECOV. 2-11-76 START & STOP DATES & IP. OIL IN NSR.
Last Compliance Report 1999-10-12 RE-ISSUE 4-23-75, R.I. & SEC. RECOV. 2-11-76 START & STOP DATES & IP. OIL IN NSR.
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Record Last Modified 2017-02-15 RE-ISSUE 4-23-75, R.I. & SEC. RECOV. 2-11-76 START & STOP DATES & IP. OIL IN NSR.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1999-10-12 0 0
0 0
2000-05-22 590 650 0
590 650 0
0 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 100 Qts 0

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-107786900 2019-7-23 0:00: ER No Violations
-1089668557 2015-10-26 0:00 ER No Violations
-1151150653 2017-11-2 0:00: ER No Violations
-1231222367 2018-1-18 0:00: ER No Violations
-1240250377 2012-12-4 0:00: ER No Violations
-1255721459 2014-5-6 0:00:0 ER No Violations
-1335985613 2017-1-5 0:00:0 ER No Violations
-139148153 2007-10-17 0:00 ER No Violations 0.50
-1395089805 2018-10-1 0:00: ER No Violations
-1412760104 2014-3-17 0:00: ER No Violations
-1553178457 2019-1-4 0:00:0 ER No Violations
-1708933932 2004-4-21 0:00: ER No Violations
-1771708998 2011-7-11 0:00: ER No Violations
-1805855384 2014-10-28 0:00 ER No Violations
-1964915538 2015-5-20 0:00: ER No Violations
-1977008786 2014-8-18 0:00: ER No Violations
-2041121013 2005-4-27 0:00: ER No Violations 0.50
-2051517616 2013-3-5 0:00:0 ER No Violations
-2067485508 2020-4-16 0:00: ER No Violations
-2125708715 2004-11-17 0:00 ER No Violations
-2142012103 2015-8-27 0:00: ER No Violations
-318023330 2008-3-13 0:00: ER No Violations 0.50
-352170252 2012-9-11 0:00: ER No Violations
-467551368 2019-11-1 0:00: ER No Violations
-613027382 2013-12-4 0:00: ER No Violations
-80913978 2016-1-4 0:00:0 ER No Violations
-840391800 2011-10-18 0:00 ER No Violations
-881778521 2012-2-27 0:00: ER No Violations
0080913978 2016-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0139148153 2007-10-17 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0159555896 2003-08-07 Enhanced Recovery Project No Violations
0318023330 2008-03-13 Enhanced Recovery Project No Violations Annulus and injection pressure test.
0339702465 2012-05-31 Enhanced Recovery Project No Violations Inspect Well.
0352170252 2012-09-11 Enhanced Recovery Project No Violations Inspect Well. Site ok.
0462289245 2016-04-15 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in poor condition.
0531040440 2013-08-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0613027382 2013-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Pump shut down during inspection.34005223470000
0689476172 2006-11-28 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0766078987 2016-07-07 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0772331268 2011-04-14 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0822635272 2018-04-09 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The Steel tubing has rusted away and the PVC liner is showing.
0840391800 2011-10-18 Enhanced Recovery Project No Violations Inspect well.
0862673049 2009-09-30 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0881778521 2012-02-27 Enhanced Recovery Project No Violations inspect well.
0947047679 2015-03-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0975806434 2016-11-01 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1068310188 2010-12-02 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1089668557 2015-10-26 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1122797788 2008-12-18 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1151150653 2017-11-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The Steel tubing has rusted away and the PVC liner is showing.
1155512446 2014-05-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Pressure test annulus to 400 psi. test held for 15 minutes with no loss in pressure. Tubing is ok.
1231222367 2018-01-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The Steel tubing has rusted away and the PVC liner is showing.
1240250377 2012-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1255721459 2014-05-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well annulus has equalized with the tubing. This well will be pressure tested for integrity.
1335985613 2017-01-05 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1376290228 2017-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The Steel tubing has rusted away and the PVC liner is showing.
1395089805 2018-10-01 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The tubing is in very poor condition.
1412760104 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1444440099 2017-04-24 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1483812514 2019-4-18 0:00: ER No Violations
1485148921 2010-04-06 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1535378226 2018-08-14 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The tubing is in very poor condition.
1539614221 2018-10-10 Work Over Reconditioning No Violations The one-inch steel tubing rusted completely away exposing the internal PVC liner. The operator attempted to pull the tubing and packer up to reset it, but the packer failed to set at a shallower depth. The tubing and packer was tripped out of the hole. A new rebuilt Parmaco packer was installed and the original 20 joints at 25 feet of Seal-tite lined tubing and one new 12.5 foot long pup joint were run in the hole. The packer was set at 512.5 feet below grade. The well bore was circulated with 150 gallons fresh water with rust inhibitor. The well head was reconstructed and pressured up to 410 pounds per square inch (psi) and monitored for 15 minutes with a loss of 10 psi. This is within the allowed margin of error and the well passed the mechanical integrity test. The operator was notified the well could be put into operation.
1553178457 2019-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
159555896 2003-8-7 0:00:0 ER No Violations
1604133999 2007-05-22 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1657273072 2013-04-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Passed test.
1708933932 2004-04-21 Enhanced Recovery Project No Violations Injection pressure test.
1771708998 2011-07-11 Enhanced Recovery Project No Violations inspect well.
1786106069 2009-04-24 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1805855384 2014-10-28 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1872410295 2005-12-01 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1921133609 2006-05-10 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1964915538 2015-05-20 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1968926069 2020-7-17 0:00: ER No Violations
1977008786 2014-08-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2041121013 2005-04-27 Enhanced Recovery Project No Violations Injection well test.
2051517616 2013-03-05 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2125708715 2004-11-17 Enhanced Recovery Project No Violations Injection pressure test.
2142012103 2015-08-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well was shut in upon inspection.
339702465 2012-5-31 0:00: ER No Violations
462289245 2016-4-15 0:00: ER No Violations
531040440 2013-8-27 0:00: ER No Violations
689476172 2006-11-28 0:00 ER No Violations 0.50
748594181 2020-1-27 0:00: ER No Violations
766078987 2016-7-7 0:00:0 ER No Violations
772331268 2011-4-14 0:00: ER No Violations 1.00
822635272 2018-4-9 0:00:0 ER No Violations
862673049 2009-9-30 0:00: ER No Violations 0.50
947047679 2015-3-19 0:00: ER No Violations
975806434 2016-11-1 0:00: ER No Violations

For data sources see[5]

References