X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-005-22220

Well Details

Well ID: 34-005-22220
Loading map...
Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: GORTNER R & P
License Status: Active Injection
License Date: 1976-02-18
Spud Date: 1976-02-17
Spud Drilling Contractor: SHORTS DRLG
Final Drill Date: 1976-09-14
Well Total Depth: 701.00 ft
Configuration: Vertical
Latitude: 40.890000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1976-02-17 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
CO 1976-02-18 133 QUAKER STATE OIL REF CORP GeoDate 2/18/76
Enhanced Recovery 1976-02-18 Issued Date 2/18/76 Expired Date 2/17/77 Acres 0203000 Tool Type CT Proposed Formation BEDFORD Proposed Depth 00000 Proposed Drill Depth 00000
Completed 1976-09-14 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
Reached Total Depth 1976-09-14 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
Construction Permit Expires 1977-02-17 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 2/18/76
Annulus Pressure Monitoring Approved 1996-07-09 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
Last Compliance Report 2001-01-10 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
Change of Owner 2007-04-27 Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC
Change of Owner 2012-11-16 Operator changed from 7578, ENERVEST OPERATING L to 8227, DEEP RESOURCES LLC
Record Last Modified 2017-02-15 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-22 554 683 0
2006-09-11 556 683 0
560 680 0
554 683 0
556 683 0
554 683 0
2000-05-22 560 680 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 254 Qts 0 WHT. WTR. TAMP.
NITR 0 254 Qts 0 FOR ERP
NITR 0 170 Qts 0 FOR PRODUCTION

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC 0.00 133.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-107637317 2013-8-29 0:00: ER No Violations
-1347910893 2018-4-23 0:00: ER No Violations
-145568931 2005-4-28 0:00: ER No Violations 0.50
-1610189177 2011-10-17 0:00 ER No Violations
-1734125552 2019-10-23 0:00 ER No Violations
-1803882646 2013-10-29 0:00 ER No Violations
-1862266217 2015-9-23 0:00: ER No Violations
-1926307451 2020-7-15 0:00: ER No Violations
-1941687240 2007-10-12 0:00 ER No Violations 0.50
-1998991993 2011-7-12 0:00: ER No Violations
-2076147986 2016-5-25 0:00: WR No Violations
-2113076327 2006-12-14 0:00 ER No Violations 1.00
-250714346 2014-7-17 0:00: ER No Violations
-354348811 2017-7-18 0:00: ER No Violations
-374395248 2019-1-14 0:00: ER No Violations
-412310811 2019-4-10 0:00: ER No Violations
-544067272 2008-12-3 0:00: ER No Violations 0.50
-635513834 2010-11-26 0:00 ER No Violations 0.50
0009989503 2013-03-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0028074834 2015-05-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well is shut in.
0050757403 2012-11-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Injection line Tee leaking.
0096408762 2016-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well was shut in upon inspection. Notified operator and injection valve was partially opened and put into production.
0107637317 2013-08-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0113455110 2009-10-07 Enhanced Recovery Project Violations Noted Injection and annulus pressure test.
0145568931 2005-04-28 Enhanced Recovery Project No Violations Injection pressure test.
0250714346 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0354348811 2017-07-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0449457198 2012-05-31 Enhanced Recovery Project No Violations Inspect Well. No Valve on Injector. Owner Name needs to be updated.
0468783087 2007-03-30 Enhanced Recovery Project No Violations Annulus and injection pressure test.
0544067272 2008-12-03 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0635513834 2010-11-26 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0700159640 2013-05-22 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0782353772 2003-11-13 Enhanced Recovery Project No Violations
0859169276 2009-04-23 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0912960573 2016-01-07 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The operator partially opened the injection valve to put well into production. Retest well to check pressure and integrity. During inspection the annulus had pressure where as there was zero pressure the previous days inspection. The packer appears to have failed.
0919503521 2014-05-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0998884457 2010-04-05 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1082806128 2017-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
113455110 2009-10-7 0:00: ER No Violations 0.50
1138293716 2006-01-26 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1174846146 2012-09-20 Enhanced Recovery Project No Violations Inspect Well. Injector Valve port stripped.
1210491559 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The valve for the annulus is frozen. Solvent tank is attached to the injection line, preventing collection of injection pressure.
1245000242 2016-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Compliance notice issued on January 8, 2015. The well has not been serviced.
1263717694 2020-5-13 0:00: ER No Violations
1344130434 2019-7-23 0:00: ER No Violations
1344382967 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The valve for the annulus was frozen during previous days inspection. Re-test annulus on well.
1347910893 2018-04-23 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1355889257 2018-07-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1389652762 2016-07-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head fittings have recently been replaced.
1415333600 2016-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1464092755 2016-05-23 Work Over Reconditioning No Violations The operator has moved the small service rig off the well and moved the large service rig onto the well. No activity is occurring on the well during the inspection. The operator reported that the packer is stuck in the hole and will not move up hole. The operator parted the one inch tubing two joins in the hole. The reaming tubing and packer have fallen to the bottom of the hole.
1465398209 2016-05-26 Work Over Reconditioning No Violations The well is constructed with 2-3/8 inch tubing at a depth of 550 feet cemented to the surface. The well is open hole from 550 feet to the total depth of 701 feet. The Berea Formation is from 556 feet to 683 feet. On May 16, 2001 the packer was set in tension reported at a depth of 525 feet with 21 joints. Compliance Notice was issued on January 8, 2016 indicating that the mechanical integrity of the well failed. Upon servicing the well the operator had difficulty removing the packer and tubing. The tubing parted at 50 feet below grade and the packer and tubing fell to the bottom of the hole. The tubing was speared and fished out of the hole. The old Butler-Larkin packer parted from the tubing and was lost in the hole and remains at the bottom of the well. A total of 22 joints at 25 feet long and one pup joint at 1.5 feet were recovered from the well. The existing Seal-tite lined tubing was reused, except five joints of tubing were in poor condition or damaged at the surface and were replaced. A new remanufactured Parmaco style unlined chrome plated packer was run in the hole in compression with 21 joints of Seal-tite lined tubing. Approximately 300 gallon of fresh water with inhibitor were pumped through the annulus and circulated out the tubing to the surface. The mechanical integrity pressure test failed at the initial depths where the packer was set. Subsequently the packer was moved up hole for retesting. The packer was set at the following depth and did not pass, 525 feet, 524 feet, and 520, feet. The operator moved the packer up hole and removed one joint of tubing. The packer was set with a total of 20 joints of tubing at a depth of 500 feet. The annulus was pressured up to 440 psi. The pressure was monitored for 15 minutes with less than 1 percent pressure loss. This is within the stated margin of 5 percent pressure loss. The well passes the Mechanical Integrity Test. The well head was reconstructed with new parts and put into production.
1509113918 2017-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1515777461 2018-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1599272904 2008-02-20 Enhanced Recovery Project Violations Noted Annulus and injection pressure test. Injection valve in box is leaking fluid. Repair valve ASAP.
1610189177 2011-10-17 Enhanced Recovery Project No Violations Inspect well. Well ownership needs review.
1617494427 2009-10-20 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1638065043 2017-04-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1655829721 2006-04-25 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1772675157 2011-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1803882646 2013-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1834944063 2008-03-13 Enhanced Recovery Project No Violations Leak has been repaired on injection line. NOV in compliance.
1862195223 2012-03-07 Enhanced Recovery Project No Violations Inspect Well. Pressure on injector line due to solvent system. No reading for injector.
1862266217 2015-09-23 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The injector has zero pressure and may be plugged. The Annulus test valve needs to be replaced, threads leak on gauge.
1876438888 2015-09-28 Administrative Inspection No Violations Operator inspected well head and determined the injection line is plugged. The well head will require replacement of all well head parts after further evaluation.
1881358711 2014-10-28 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1883099978 2015-10-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Operator reported there was a tubing line plug that was cleaned out and well head fitting were repaired and replaced.
1940579143 2004-04-22 Enhanced Recovery Project No Violations Injection pressure test. Annular pressure needs re-tested and reported to Tom Tomastik in 30 days. Advised Len Rex to repressure annular space.
1941687240 2007-10-12 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1966039779 2020-1-17 0:00: ER No Violations
1998991993 2011-07-12 Enhanced Recovery Project No Violations inspect well. Conduct mini test, ok.
2050497528 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
2076147986 2016-05-25 Work Over Reconditioning No Violations Operator reported that 22 joints of one inch Seal-tite lined tubing and one 18 inch long pup joint of tubing were recover from the well. The packer was lost in the hole.
2113076327 2006-12-14 Enhanced Recovery Project No Violations Injection and annulus pressure test. Surface valves and 1 tubing rusted and scaled. It is not leaking.
2126643091 2018-10-12 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
28074834 2015-5-13 0:00: ER No Violations
449457198 2012-5-31 0:00: ER No Violations
468783087 2007-3-30 0:00: ER No Violations
50757403 2012-11-27 0:00 ER No Violations
700159640 2013-5-22 0:00: ER No Violations
782353772 2003-11-13 0:00 ER No Violations
859169276 2009-4-23 0:00: ER No Violations 0.50
912960573 2016-1-7 0:00:0 ER No Violations
919503521 2014-5-27 0:00: ER No Violations
96408762 2016-1-6 0:00:0 ER No Violations
998884457 2010-4-5 0:00:0 ER No Violations 0.50
9989503 2013-3-4 0:00:0 ER No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0113455110 US-OH-103410 2009-10-07 Failure to conduct or pass mech. integrity test
0912960573 US-OH-130422 2016-06-15 Mechanical failure/contamination
1599272904 US-OH-115669 2008-02-20 Pollution/Contamination

For data sources see[9]

References