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Well ID: 34-005-21104 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Hanover Township | |
Operator Name: COLUMBIA GAS TRANSMISSION LLC | |
Well Pad ID: | |
Farm/Lease Name: STATE OF OHIO | |
License Status: Storage Well | |
License Date: | |
Spud Date: 1954-11-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1954-12-29 | |
Well Total Depth: 2857.00 ft | |
Configuration: Vertical | |
Latitude: 40.600000 | |
Longitude: -82.310000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1954-11-13 | |
Completed | 1954-12-29 | |
Reached Total Depth | 1954-12-29 | |
Record Last Modified | 2013-05-23 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2014-08-11 | H2O | 0 | 12320 Gal | 15500 | Universal Well Services Inc. | The job utilized cross linked fresh water gel fluid. Approximately 43,000 cubic ft of nitrogen gas was pumped with the job. This was a refracture cleanout of the formation and no break was noted on the job. The formation refused sand during the job and caused pressure to ramp above the 3000psi top pressure. The job was shut down and not all of the sand was pumped to the formation. The well bore is loaded with sand and is going to need to be cleaned out. |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1510803428 | 2017-10-2 0:00: | SO | No Violations | |
-1901392713 | 2014-8-11 0:00: | WR | No Violations | 2.50 |
-381287351 | 2016-11-17 0:00 | SO | No Violations | 0.50 |
-958437100 | 2018-11-5 0:00: | SO | No Violations | |
0381287351 | 2016-11-17 | Storage Well | No Violations | ID is posted and the location is maintained. The annulus is shut in and the valves have bull plugs in them. |
0473917625 | 2019-03-28 | Storage Well | No Violations | Inspect well, identification is posted. A pig launcher is in line at the wellhead. |
0958437100 | 2018-11-05 | Storage Well | No Violations | ID is posted and the location is maintained. The annulus is open. |
1173356702 | 2015-11-23 | Storage Well | No Violations | ID is posted and the location is maintained. The annulus is shut in. There is no separator at this well. |
1176302125 | 2014-02-10 | Storage Well | No Violations | ID posted, location maintained. |
1510803428 | 2017-10-02 | Storage Well | No Violations | ID is posted and the location is maintained. The annulus is open. There is no separator at the well. |
1703986717 | 2020-5-7 0:00:0 | SO | No Violations | |
1901392713 | 2014-08-11 | Work Over Reconditioning | No Violations | The operator requested inspection to witness fracture stimulation of the well. See the stimulation report for details. |
358889055 | 2019-6-6 0:00:0 | SO | No Violations | |
473917625 | 2019-3-28 0:00: | SO | No Violations |
For data sources see[4]