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Difference between revisions of "34-121-23136"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-121-23136
 
| Well ID: 34-121-23136
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.60352319, -81.4940405 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.603449782, -81.49419509 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Noble County, Ohio|Noble]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Noble_County,_Ohio|Noble]]
 +
|-
 +
| Municipality: [[Jackson_Township,_Noble_County,_Ohio|Jackson Township]]
 
|-
 
|-
 
| Operator Name: [[NORTHWOOD ENERGY CORP]]
 
| Operator Name: [[NORTHWOOD ENERGY CORP]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: ATHERTON CLARK
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2014-07-02
 
|-
 
|-
 
| Spud Date: 1984-05-29
 
| Spud Date: 1984-05-29
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[MID ATLANTC DRLG]]
|-
 
| Configuration: Vertical
 
 
|-
 
|-
| Well Status: Final Restoration
+
| Final Drill Date: 1984-06-16
 
|-
 
|-
| Violations: 0
+
| Well Total Depth: 6332 ft
 
|-
 
|-
| Latitude: 39.60352319
+
| Configuration: Vertical
 
|-
 
|-
| Longitude: -81.4940405
+
| Latitude: 39.603449782
 
|-
 
|-
 +
| Longitude: -81.49419509
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Well Status
!scope="col" | GAS QUANTITY
+
!scope="col" style="width: 15%;text-align: center"| Well Status Date
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comment
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
 
|-
 
|-
| 1984-0
+
| CO
| style="text-align:right;" | 10522.0
+
| 1984-02-08
 +
| 3443  MALVERN GROUP INC  GeoDate  2/8/84
 +
|-
 +
| Oil and Gas
 +
| 1984-02-08
 +
| Issued Date 2/8/84 Expired Date 8/6/84 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06332 Proposed Drill Depth 06332
 +
|-
 +
| Original Spud
 +
| 1984-05-29
 
|  
 
|  
 +
|-
 +
| Completed
 +
| 1984-06-16
 
|  
 
|  
 +
|-
 +
| Reached Total Depth
 +
| 1984-06-16
 
|  
 
|  
| style="text-align:right;" | 0.0
+
|-
 +
| Completion Report Received
 +
| 1984-07-12
 
|  
 
|  
 
|-
 
|-
 +
| APP
 +
| 1999-03-17
 +
| Proposed Formations:CLINTON, Issued Date:3/17/99, Expired Date:3/16/00 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
 +
|-
 +
| Change of Owner
 +
| 2000-02-14
 +
| Operator changed from 3443, MALVERN GROUP INC to 6351, T  &  C OIL & GAS COMPANY
 +
|-
 +
| Change of Owner
 +
| 2000-04-05
 +
| Operator changed from 6351, T  &  C OIL & GAS COMPANY to 6733, C & M GAS & OIL
 +
|-
 +
| Change of Owner
 +
| 2001-04-18
 +
| Operator changed from 6733, C & M GAS & OIL to 4431, VALLEY ENTERPRISES
 
|-
 
|-
| 1985-0
+
| APP
| style="text-align:right;" | 16495.0
+
| 2008-04-22
 +
| Proposed Formations:CLINTON, Issued Date:4/22/2008, Expired Date:4/22/2009 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:HAD, Proposed Well Class:
 +
|-
 +
| Change of Owner
 +
| 2008-10-21
 +
| Operator changed from 4431, VALLEY ENTERPRISES to 1634, NORTHWOOD ENERGY CORP
 +
|-
 +
| APP
 +
| 2010-07-01
 +
| Proposed Formations:DEVONIAN SHALE THRU ORISKANY, Issued Date:7/1/2010, Expired Date:7/1/2011 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class:ENPW
 +
|-
 +
| APP
 +
| 2014-03-14
 +
| Proposed Formations:ORISKANY, Issued Date:3/14/2014, Expired Date:3/13/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class:
 +
|-
 +
| Plugged/Abandoned
 +
| 2014-05-05
 
|  
 
|  
 +
|-
 +
| Construction Permit Expires
 +
| 2016-03-13
 
|  
 
|  
 +
|-
 +
| Record Last Modified
 +
| 2017-10-13
 
|  
 
|  
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
| 1997-06-29
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" |
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2006-09-11
 +
| style="text-align: right;" | 6081
 +
| style="text-align: right;" | 6214
 +
| style="text-align: right;" | 40
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1986-0
 
| style="text-align:right;" | 2141.0
 
 
|  
 
|  
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 52750 Gal
 +
| style="text-align: right;" | 50000
 
|  
 
|  
 +
| FRAC;H2O,SAND
 +
|-
 
|  
 
|  
| style="text-align:right;" | 0.0
+
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 36500 Gal
 +
| style="text-align: right;" | 40000
 
|  
 
|  
 +
| MED.
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 1987-0
+
| 1984
| style="text-align:right;" | 5854.0
+
| [[DERBY OIL & GAS CORP]]
|  
+
| style="text-align: right;" | 10522
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
|-
|  
+
| 1985
 +
| [[DERBY OIL & GAS CORP]]
 +
| style="text-align: right;" | 16495
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 353
 +
|-
 +
| 1986
 +
| [[DERBY OIL & GAS CORP]]
 +
| style="text-align: right;" | 2141
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 357
 +
|-
 +
| 1987
 +
| [[CHRISTA OIL CO]]
 +
| style="text-align: right;" | 5854
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 361
 +
|-
 +
| 1988
 +
| [[BAUGHMAN ELEANOR]]
 +
| style="text-align: right;" | 2091
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 356
 +
|-
 +
| 1989
 +
| [[BAUGHMAN ELEANOR]]
 +
| style="text-align: right;" | 994
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 334
 +
|-
 +
| 1990
 +
| [[MALVERN GROUP INC]]
 +
| style="text-align: right;" | 2865
 +
| style="text-align: right;" | 6
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1991
 +
| [[MALVERN GROUP INC]]
 +
| style="text-align: right;" | 2127
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 363
 +
|-
 +
| 1992
 +
| [[MALVERN GROUP INC]]
 +
| style="text-align: right;" | 2477
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 1993
 +
| [[MALVERN GROUP INC]]
 +
| style="text-align: right;" | 2372
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1988-0
+
| 1994
| style="text-align:right;" | 2091.0
+
| [[MALVERN GROUP INC]]
|  
+
| style="text-align: right;" | 2452
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1995
 +
| [[MALVERN GROUP INC]]
 +
| style="text-align: right;" | 2458
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1989-0
+
| 1996
| style="text-align:right;" | 994.0
+
| [[MALVERN GROUP INC]]
|  
+
| style="text-align: right;" | 2364
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1997
 +
| [[MALVERN GROUP INC]]
 +
| style="text-align: right;" | 2272
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1990-0
+
| 1998
| style="text-align:right;" | 2865.0
+
| [[MALVERN GROUP INC]]
|  
+
| style="text-align: right;" | 1053
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 6.0
 
|
 
 
|-
 
|-
 +
| 1999
 +
| [[MALVERN GROUP INC]]
 +
| style="text-align: right;" | 120
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 60
 
|-
 
|-
| 1991-0
+
| 2000
| style="text-align:right;" | 2127.0
+
| [[MALVERN GROUP INC]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[VALLEY ENTERPRISES]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1992-0
+
| 2008
| style="text-align:right;" | 2477.0
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1993-0
+
| 2010
| style="text-align:right;" | 2372.0
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 121
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1994-0
+
| 2012
| style="text-align:right;" | 2452.0
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 59
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1995-0
+
| 2014
| style="text-align:right;" | 2458.0
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 91
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 1996-0
+
| 1984
| style="text-align:right;" | 2364.0
+
| [[DERBY OIL & GAS CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 472
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1985
 +
| [[DERBY OIL & GAS CORP]]
 +
| Brine
 +
| style="text-align: right;" | 450
 +
| style="text-align: right;" | 353
 
|-
 
|-
| 1997-0
+
| 1986
| style="text-align:right;" | 2272.0
+
| [[DERBY OIL & GAS CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 142
|
+
| style="text-align: right;" | 357
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1987
 +
| [[CHRISTA OIL CO]]
 +
| Brine
 +
| style="text-align: right;" | 150
 +
| style="text-align: right;" | 361
 
|-
 
|-
| 1998-0
+
| 1988
| style="text-align:right;" | 1053.0
+
| [[BAUGHMAN ELEANOR]]
|  
+
| Brine
|
+
| style="text-align: right;" | 142
|
+
| style="text-align: right;" | 356
|
 
|  
 
 
|-
 
|-
 +
| 1989
 +
| [[BAUGHMAN ELEANOR]]
 +
| Brine
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 334
 
|-
 
|-
| 1999-0
+
| 1990
| style="text-align:right;" | 120.0
+
| [[MALVERN GROUP INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 72
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1991
 +
| [[MALVERN GROUP INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 363
 
|-
 
|-
| 2000-0
+
| 1992
| style="text-align:right;" | 0.0
+
| [[MALVERN GROUP INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1993
 +
| [[MALVERN GROUP INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 1994
| style="text-align:right;" | 0.0
+
| [[MALVERN GROUP INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1995
 +
| [[MALVERN GROUP INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2008-0
+
| 1996
| style="text-align:right;" | 0.0
+
| [[MALVERN GROUP INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1997
 +
| [[MALVERN GROUP INC]]
 +
| Brine
 +
| style="text-align: right;" |
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2009-0
+
| 1998
| style="text-align:right;" | 0.0
+
| [[MALVERN GROUP INC]]
|
+
| Brine
|
+
| style="text-align: right;" |  
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1999
 +
| [[MALVERN GROUP INC]]
 +
| Brine
 +
| style="text-align: right;" |
 +
| style="text-align: right;" | 60
 
|-
 
|-
| 2010-0
+
| 2000
| style="text-align:right;" | 0.0
+
| [[MALVERN GROUP INC]]
|
+
| Brine
|
+
| style="text-align: right;" |  
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[VALLEY ENTERPRISES]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2011-0
+
| 2008
| style="text-align:right;" | 121.0
+
| [[NORTHWOOD ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2012-0
+
| 2010
| style="text-align:right;" | 0.0
+
| [[NORTHWOOD ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" |
 
|-
 
|-
| 2013-0
+
| 2012
| style="text-align:right;" | 0.0
+
| [[NORTHWOOD ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 75
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 59.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 107
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2014-0
+
| 2014
| style="text-align:right;" | 0.0
+
| [[NORTHWOOD ENERGY CORP]]
| style="text-align:right;" | 365.0
+
| Brine
|  
+
| style="text-align: right;" | 340
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 91.0
 
| style="text-align:right;" | 365.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2019-05-07
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| -126321449
+
| 0000PL7609
 +
|
 +
| Preliminary Restoration
 +
| No Violations
 +
| Preliminary Restoration  done information from Data Point
 +
|-
 +
| 0126321449
 
| 2004-03-23
 
| 2004-03-23
|  
+
| Production Wells
| Inspection revealed wel to be idle no I.D.posted 4x2 swedge on top valves shut as phot's indicate
+
| No Violations
 +
| Inspection revealed wel to be idle no I.D.posted 4x2 swedge on top valves shut as phots indicate
 
H2S gas odor present.
 
H2S gas odor present.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1362360061
 
| 1362360061
 
| 2014-05-02
 
| 2014-05-02
|  
+
| Plug / Plug Back
 +
| No Violations
 
| My inspection today finds the service rig crew pulled the collar off of the 4.5 casing while trying to rip the pipe.  The cement crew was sent back.
 
| My inspection today finds the service rig crew pulled the collar off of the 4.5 casing while trying to rip the pipe.  The cement crew was sent back.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1399049324
 
| 1399049324
 
| 2014-05-01
 
| 2014-05-01
|  
+
| Plug / Plug Back
| My inspection today finds Davis Well Service moved a rig onto the location.  The rig crew ran the wire line tools in the well and found the top of the lime plug at 4042'.
+
| No Violations
|
+
| My inspection today finds Davis Well Service moved a rig onto the location.  The rig crew ran the wire line tools in the well and found the top of the lime plug at 4042.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1399309060
 
| 1399309060
 
| 2014-05-05
 
| 2014-05-05
|  
+
| Plug / Plug Back
| My inspection today finds the casing was ripped at 3660'.  Cemenco circulated a 38 sk class A 2% gel plug.  The casing was pulled up to 1950'.  Cemenco circulated a 52 sk 2% gel plug into place.  A 200' 54 sk plug was placed from 200' to surface.  I instructed the company to reclaim the site in accordance with 1509.072.
+
| No Violations
|
+
| My inspection today finds the casing was ripped at 3660.  Cemenco circulated a 38 sk class A 2% gel plug.  The casing was pulled up to 1950.  Cemenco circulated a 52 sk 2% gel plug into place.  A 200 54 sk plug was placed from 200 to surface.  I instructed the company to reclaim the site in accordance with 1509.072.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1668780202
 
| 1668780202
 
| 2014-07-02
 
| 2014-07-02
|  
+
| Final Restoration
 +
| No Violations
 
| Site has met 1509.072B restoration requirements. There was no evidence of production equipment left behind.
 
| Site has met 1509.072B restoration requirements. There was no evidence of production equipment left behind.
|
 
|
 
|
 
 
|-
 
|-
 +
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| PL7609
+
|}-->
|
 
|
 
| Preliminary Restoration  done information from Data Point
 
|
 
|
 
|
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 03:47, 24 July 2019

Well Details

Well ID: 34-121-23136
Loading map...
Country: United States
State: Ohio
County: Noble
Municipality: Jackson Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: ATHERTON CLARK
License Status: Final Restoration
License Date: 2014-07-02
Spud Date: 1984-05-29
Spud Drilling Contractor: MID ATLANTC DRLG
Final Drill Date: 1984-06-16
Well Total Depth: 6332 ft
Configuration: Vertical
Latitude: 39.603449782
Longitude: -81.49419509

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-02-08 3443 MALVERN GROUP INC GeoDate 2/8/84
Oil and Gas 1984-02-08 Issued Date 2/8/84 Expired Date 8/6/84 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06332 Proposed Drill Depth 06332
Original Spud 1984-05-29
Completed 1984-06-16
Reached Total Depth 1984-06-16
Completion Report Received 1984-07-12
APP 1999-03-17 Proposed Formations:CLINTON, Issued Date:3/17/99, Expired Date:3/16/00 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2000-02-14 Operator changed from 3443, MALVERN GROUP INC to 6351, T & C OIL & GAS COMPANY
Change of Owner 2000-04-05 Operator changed from 6351, T & C OIL & GAS COMPANY to 6733, C & M GAS & OIL
Change of Owner 2001-04-18 Operator changed from 6733, C & M GAS & OIL to 4431, VALLEY ENTERPRISES
APP 2008-04-22 Proposed Formations:CLINTON, Issued Date:4/22/2008, Expired Date:4/22/2009 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:HAD, Proposed Well Class:
Change of Owner 2008-10-21 Operator changed from 4431, VALLEY ENTERPRISES to 1634, NORTHWOOD ENERGY CORP
APP 2010-07-01 Proposed Formations:DEVONIAN SHALE THRU ORISKANY, Issued Date:7/1/2010, Expired Date:7/1/2011 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class:ENPW
APP 2014-03-14 Proposed Formations:ORISKANY, Issued Date:3/14/2014, Expired Date:3/13/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class:
Plugged/Abandoned 2014-05-05
Construction Permit Expires 2016-03-13
Record Last Modified 2017-10-13

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 0 0
2006-09-11 6081 6214 40

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 52750 Gal 50000 FRAC;H2O,SAND
H2O 0 36500 Gal 40000 MED.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 DERBY OIL & GAS CORP 10522 0 0
1985 DERBY OIL & GAS CORP 16495 0 353
1986 DERBY OIL & GAS CORP 2141 0 357
1987 CHRISTA OIL CO 5854 0 361
1988 BAUGHMAN ELEANOR 2091 0 356
1989 BAUGHMAN ELEANOR 994 0 334
1990 MALVERN GROUP INC 2865 6 365
1991 MALVERN GROUP INC 2127 0 363
1992 MALVERN GROUP INC 2477 0 365
1993 MALVERN GROUP INC 2372 0 365
1994 MALVERN GROUP INC 2452 0 365
1995 MALVERN GROUP INC 2458 0 365
1996 MALVERN GROUP INC 2364 0 365
1997 MALVERN GROUP INC 2272 0 365
1998 MALVERN GROUP INC 1053 0 365
1999 MALVERN GROUP INC 120 0 60
2000 MALVERN GROUP INC 0 0 0
2001 VALLEY ENTERPRISES 0 0 0
2008 NORTHWOOD ENERGY CORP 0 0 0
2009 NORTHWOOD ENERGY CORP 0 0 0
2010 NORTHWOOD ENERGY CORP 0 0 0
2011 NORTHWOOD ENERGY CORP 121 0 0
2012 NORTHWOOD ENERGY CORP 0 0 0
2013 NORTHWOOD ENERGY CORP 0 59 365
2014 NORTHWOOD ENERGY CORP 0 91 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 DERBY OIL & GAS CORP Brine 472 0
1985 DERBY OIL & GAS CORP Brine 450 353
1986 DERBY OIL & GAS CORP Brine 142 357
1987 CHRISTA OIL CO Brine 150 361
1988 BAUGHMAN ELEANOR Brine 142 356
1989 BAUGHMAN ELEANOR Brine 100 334
1990 MALVERN GROUP INC Brine 72 365
1991 MALVERN GROUP INC Brine 0 363
1992 MALVERN GROUP INC Brine 0 365
1993 MALVERN GROUP INC Brine 0 365
1994 MALVERN GROUP INC Brine 0 365
1995 MALVERN GROUP INC Brine 0 365
1996 MALVERN GROUP INC Brine 0 365
1997 MALVERN GROUP INC Brine 365
1998 MALVERN GROUP INC Brine 365
1999 MALVERN GROUP INC Brine 60
2000 MALVERN GROUP INC Brine 0
2001 VALLEY ENTERPRISES Brine 0 0
2008 NORTHWOOD ENERGY CORP Brine 0 0
2009 NORTHWOOD ENERGY CORP Brine 0 0
2010 NORTHWOOD ENERGY CORP Brine 0 0
2011 NORTHWOOD ENERGY CORP Brine 0
2012 NORTHWOOD ENERGY CORP Brine 75 0
2013 NORTHWOOD ENERGY CORP Brine 107 365
2014 NORTHWOOD ENERGY CORP Brine 340 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000PL7609 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0126321449 2004-03-23 Production Wells No Violations Inspection revealed wel to be idle no I.D.posted 4x2 swedge on top valves shut as phots indicate

H2S gas odor present.

1362360061 2014-05-02 Plug / Plug Back No Violations My inspection today finds the service rig crew pulled the collar off of the 4.5 casing while trying to rip the pipe. The cement crew was sent back.
1399049324 2014-05-01 Plug / Plug Back No Violations My inspection today finds Davis Well Service moved a rig onto the location. The rig crew ran the wire line tools in the well and found the top of the lime plug at 4042.
1399309060 2014-05-05 Plug / Plug Back No Violations My inspection today finds the casing was ripped at 3660. Cemenco circulated a 38 sk class A 2% gel plug. The casing was pulled up to 1950. Cemenco circulated a 52 sk 2% gel plug into place. A 200 54 sk plug was placed from 200 to surface. I instructed the company to reclaim the site in accordance with 1509.072.
1668780202 2014-07-02 Final Restoration No Violations Site has met 1509.072B restoration requirements. There was no evidence of production equipment left behind.

For data sources see[9]

References