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37-131-20161

Well Details

Well ID: 37-131-20161
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Country: United States
State: Pennsylvania
County: Wyoming
Municipality: Nicholson Township
Operator Name: CHIEF OIL & GAS LLC
Well Pad ID: 149079
Farm/Lease Name: POLOVITCH UNIT
License Status: Plugged and Abandoned
Spud Date: 2011-06-14
Permit Date: 2011-05-04
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.640753
Longitude: -75.810942

For data sources see[1][2][3]

Well History

Date Event
2011-05-04 New Permit Application
2011-06-12 Performed Spud Operation
2011-07-12 Drilling Completion
2011-09-29 DEVIATED
2015-07-27 Begin Plugging
2018-11-08 Finished Plugging
2018-12-13 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2011 CHIEF OIL & GAS LLC 0.00 0 0.00 0 0.00 0
2012 CHIEF OIL & GAS LLC 0.00 0 0.00 0 0.00 0
2013 CHIEF OIL & GAS LLC 0.00 0 0.00 0 0.00 0
2014 CHIEF OIL & GAS LLC 0.00 0 0.00 0 0.00 0
2015 CHIEF OIL & GAS LLC 0.00 0 0.00 0 0.00 0
2016 CHIEF OIL & GAS LLC 0.00 0 0.00 0 0.00 0
2017 CHIEF OIL & GAS LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2011 CHIEF OIL & GAS LLC Fracing Fluid Waste 600.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE EPA ID: 748-163
2011 CHIEF OIL & GAS LLC Drilling Fluid Waste 360.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE EPA ID: 748-163
2011 CHIEF OIL & GAS LLC Drill Cuttings 363.69 Tons LANDFILL 301626
2011 CHIEF OIL & GAS LLC Fracing Fluid Waste 119.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0008451
2018 CHIEF OIL & GAS LLC Spent Lubricant Waste 12.81 Bbl LANDFILL 301358

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1980302 Primary Facility 2011-06-13 Drilling/Alteration No Violations Noted Ziegenfuss on site. Current depth 30' - no water.
1981708 Primary Facility 2011-06-20 Drilling/Alteration No Violations Noted "20" at 140' sanded in UDI Rig 58, Comp. Man - Kenny George
1984434 Primary Facility 2011-06-24 Drilling/Alteration No Violations Noted Comp. Man - Jim Quisenberry Drillers log good at 2512'
1985110 Primary Facility 2011-07-01 Drilling/Alteration No Violations Noted UDI #58, depth = 7138'
1986572 Primary Facility 2011-07-07 Drilling/Alteration No Violations Noted UDI Rig 58, Comp. Man - Kenny George
1987802 Primary Facility 2011-07-11 Drilling/Alteration No Violations Noted getting ready to cement 5 1/2" prod csg.
1990418 Primary Facility 2011-07-25 Routine/Complete Inspection No Violations Noted Vent pipe on 5 1/2" X 95/8" annulus runs to frac tank.
2005966 Primary Facility 2011-09-27 Routine/Complete Inspection No Violations Noted
2026318 Primary Facility 2011-12-09 Complaint Inspection Pending This well is not in production (others on site are). There are 2 vents, cellar is filled with gravel. There is 46 psi on annulus vent.? which annulus? Cellar is filled w/ gravel.
2029333 Primary Facility 2011-12-15 Complaint Inspection Pending This well is not in prod. There are 2 annular vents, but cellar is filled in. Eric Rooney took isotopic samples.
2029338 Primary Facility 2011-12-19 Follow-up Inspection Violation(s) Noted Went with Kevin Costello and met with Rich Adams/Chief rep. Cellar has been dug up to identify which annulus the vents go to.
2029343 Primary Facility 2011-12-22 Follow-up Inspection Outstanding Violations - No Viols Req'd On site to take flow readings w/ oriface meter. Met Ralph Larson, and Jon Hafer / Chief reps.
2051400 Primary Facility 2012-03-15 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Cellar is dug out, no water. Orange fence is on ground.
2062425 Primary Facility 2012-04-12 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Well is not producing. Cellar is partially dug out, no water.
2062432 Primary Facility 2012-03-27 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Not producing. Cellar dug out, no water. 3 vents.
2064981 Primary Facility 2012-04-27 Routine/Complete Inspection Outstanding Violations - No Viols Req'd 3 annular vents, no guages, open.
2067576 Primary Facility 2012-05-14 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Well is not producing. 3 annular vents - open. Cellar partially dug out - no water.
2076977 Primary Facility 2012-06-18 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Not producing. Has 3 annular vents, all are shut w/ temp., press.recorders installed. The #1 vent (13 3/8 X 9 5/8") alsohas press. guage w/ 180 psi.
2078692 Primary Facility 2012-06-20 Follow-up Inspection Outstanding Violations - No Viols Req'd No water in cellar. All press/temp recorders have been removed and vents have been opened. Talked to Rich Adams, Chief, and he says bubbles were from leaky valve under gravel. Cellar will be dug up and flooded to check, soon. Also, Chief will have data for us soon and set up meeting to discus and see how to procede( a week or so).
2080477 Primary Facility 2012-06-26 Follow-up Inspection Outstanding Violations - No Viols Req'd no change since last inspection.
2081757 Primary Facility 2012-07-09 Follow-up Inspection Outstanding Violations - No Viols Req'd Cellars dug out. No change since last insp. The valve on the annular vent is exposed, don't know(can't tell) if it leaks. None of the wells have press. recorders. Called R. Adams(Chief) to see what progress they are making on VIOS. He called back that we will hear from them- not quite ready with info. Also check on leaky valve - will call when flooding cellar.
2084484 Primary Facility 2012-07-03 Follow-up Inspection Outstanding Violations - No Viols Req'd Cellar has been dug out. No water. There is a valve on line but can't tell if it leaks. Cellar on 4H has also been dug out.
2086661 Primary Facility 2012-07-24 Follow-up Inspection Outstanding Violations - No Viols Req'd No change since last insp.
2087770 Primary Facility 2012-07-30 Follow-up Inspection Outstanding Violations - No Viols Req'd Not a prod. well. 3 annular vents, open. Muddy water in cellar, no bubbles. No press guages. No change since last insp.
2097231 Primary Facility 2012-08-30 Follow-up Inspection Outstanding Violations - No Viols Req'd On site w/ Kevin Costello(DEP), Ralph Larsen(Chief) & Jon Hafer(Chief Consultant) to witness flow tests and pressure test on annuli. Shut in 3 annuli for 20 min. - 9 5/8 x 5 1/2" = 0 psi, 9 5/8 x 13 3/8" = 10 psi, and 20 x 13 3/8" = 0 psi.
2103126 Primary Facility 2012-09-14 Follow-up Inspection Outstanding Violations - No Viols Req'd No change since last insp. Cellar is dug out - very small amount of water in cellar - no bubbles. 3 annular vents, no pressure guages, all are vented to tanks.
2112198 Primary Facility 2012-10-24 Follow-up Inspection Outstanding Violations - No Viols Req'd Equip. & people on site - finishing up pipeline work & moving out equipment.
2175536 Primary Facility 2013-06-11 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Well is not producing. 3 annular vents are open.
2196363 Primary Facility 2013-08-14 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Not producing. Water in cellar.
2213504 Primary Facility 2013-10-01 Follow-up Inspection Outstanding Violations - No Viols Req'd On site w/ Eric Rooney, DEP and Jon Hafer, Chief to collect isotopic samples from various annuli. Shut in for 17+ hours, since about 4:30PM yesterday.
2240193 Primary Facility 2014-01-24 Routine/Complete Inspection Outstanding Violations - No Viols Req'd No activity on site.
2263075 Primary Facility 2014-04-11 Routine/Complete Inspection No Violations Noted Well has been drilled and we have recieved a well record, but has not been completeds. It is still on active status in e- facts.
2321207 Primary Facility 2014-11-04 Follow-up Inspection Violation(s) Noted
2670039 Primary Facility 2017-12-11 Follow-up Inspection No Violations Noted There was no activity occurring at the site during the inspection. I was accompanied by Jon Sassi (OGI) and consulted with Ken Kennedy (OGI). There were no violations noted pertaining to this well. If you have any questions, please contact me.
2703214 Primary Facility 2018-02-22 Compliance Evaluation In Compliance with Schedule Arrived onsite at 15:15. Onsite to check on progress of re plumbing of all (4) wells annular vents to surface in preparation for long term venting phase as discussed and agreed to in the Depts. meeting with Chief O&G of 2/14/18. All (4) wells, the Polovitch 1H, 1V, 4H and 5H, have had their (20" x 13 3/8"), (13 3/8" x 9 5/8") and (9 5/8" / WB) annular vents plumbed to surface via 2" vents. Vents had been fitted with ball valves and Tees w/ needle valves to access vents for sampling and eventual PBUTs. The Dept. will be meeting Chief O&G Rep., Jon Hafer back at pad tomorrow morning at 09:30 to obtain gas samples off all annuli, where gas is present, for Isotopic analysis. Chief O&G has had all annular spaces and vents purged of fluid and were shut in earlier today in preparation for tomorrows sampling event. (See attached, "As Plugged" Well Bore Schematics for individual wells for plugging details as of 2/14/18). All previous, deteriorated pad liner and debris have been removed from location. Location was fou
2703226 Primary Facility 2018-02-23 Compliance Evaluation In Compliance with Schedule Arrived onsite at 09:00. Upon arrival met up with Chief O&G Rep., Jonathan Hafer and D.E.P. Geologist, Eric Rooney. Onsite to initiate the 1st long term, approx. 90 day, venting period as agreed to in meeting of 2/14/18 with Chief O&G. All (4) wells annuli vents, the (20" x 13 3/8"), (13 3/8" x 9 5/8") and (9 5/8" / WB) were re-plumbed to surface and shut-in yesterday in preparation for todays sampling. Mr. Hafer explained that he would be taking gas samples off all the wells annular vents to send off for analysis. Following Mr. Hafers collection of annuli samples, I performed gas screenings at all (4) wells annuli using a ALTAIR 5X gas meter calibrated on 2/5/18. Gas was detected at the following wells annuli:

1H: (13 x 9) = 100% LEL, 100% CH4, 4H: (13 x 9) = 100 % LEL, 30 % CH4, 5H: (13 x 9) = 100 % LEL, 8 % CH4, Following sample collection and gas screenings, all (4) wells annuli were opened to vent to atmosphere. This long term venting period will extend for ~ 90 days. Operator will then be performing

2775963 Primary Facility 2018-08-31 Compliance Evaluation In Compliance with Schedule Arrived onsite at 11:00. Upon arrival met with Chief O&G Rep., Jonathan Hafer to conclude the 7 day PBUTs being performed on all (4) wells annuli vents, the (20" x 13 3/8"), (13 3/8" x 9 5/8") and (9 5/8" / WB). This is the 2nd PBUT being performed after (2) full 90 day, long term venting periods. Pre-shut in test gas screenings were performed at all wells annular vents on 8/24/18 by Mr. Hafer using a Rae Systems Multi-Rae gas meter, calibrated that morning. The only annuli where gas was detected are listed below:

1H: (13x9) = 3.1% CH4, 51% LEL 1V: (9/WB) = 1.6% CH4, 36% LEL 4H: (13x9) = 1.9% CH4, 70% LEL 5H: (13x9) = 6.6% CH4, 100% LEL

Today, the ending 7 day PBUT results were: 1H: (20x13)= 0.40 psi, (13x9)= 12.95 psi, (9/WB)= 0.44 psi. 1V: (20x13)= -0.10 psi, (13x9)= -2.0 psi, (9/WB)= 0.45 psi. 4H: (20x13)= 0.10 psi, (13x9)= 11.10 psi, (9/WB)= 0.70 psi. 5H: (20x13)= 0.65 psi, (13x9)= 5.2 psi, (9/WB)= 0.75psi. - Mr. Hafer explained that he would be collecting samples off all the wells annular vents to sen

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2029338 627794 12/19/2011 2011-12-19 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days Administrative GMI COA executed 10/23/2017
2321207 710152 11/04/2014 2014-11-04 78.73A - Operator shall prevent gas and other fluids from lower formations from entering fresh groundwater. Environmental Health & Safety Actually 78.73(b)
2321207 710153 11/04/2014 2014-11-04 78.81D1 - Failure to maintain control of anticipated gas storage reservoir pressures while drilling through reservoir or protective area Administrative Actually 78.81 (a)(2)+(3)
2321207 710155 11/04/2014 2014-11-04 78.85 - Inadequate, insufficient, and/or improperly installed cement Environmental Health & Safety Actually 78.85(a)(5)
2321207 710156 11/04/2014 2014-11-04 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days Administrative
2321207 799777 11/04/2014 2014-11-04 CSL 401 - PROHIBITION AGAINST OTHER POLLUTIONS - Discharged substance of any kind or character resulting in pollution of Waters of the Commonwealth. Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
627794 279011 NOV - Notice of Violation
710152 317500 NOV - Notice of Violation
710152 358810 COA - Consent Order and Agreement 2017-10-23 $178,622.00 $178,622.00
710153 317500 NOV - Notice of Violation
710153 358810 COA - Consent Order and Agreement 2017-10-23 $178,622.00 $178,622.00
710155 317500 NOV - Notice of Violation
710156 317500 NOV - Notice of Violation
710156 358810 COA - Consent Order and Agreement 2017-10-23 $178,622.00 $178,622.00
799777 317500 NOV - Notice of Violation Administrative Close Out 2017-10-23
799777 358810 COA - Consent Order and Agreement 2017-10-23 $178,622.00 $178,622.00

For data sources see[7]

References