X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-131-20141

Well Details

Well ID: 37-131-20141
Loading map...
Country: United States
State: Pennsylvania
County: Wyoming
Municipality: Washington Township
Operator Name: CARRIZO (MARCELLUS) LLC
Well Pad ID:
Farm/Lease Name: SICKLER 5H
License Status:
Spud Date:
Permit Date: 2011-03-03
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.608483
Longitude: -75.973228

For data sources see[1][2][3]

Well History

Date Event
2011-03-03 New Permit Application
2011-07-15 Drilling Completion
2012-06-13 DEVIATED

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2012-06-11 2012-06-11 8,030 3,075,156

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 Sand, White, 100 Baker Hughes Proppant Quartz 14808-60-7 100.00 0.88
Hydrochloric Acid 10.1-15 Baker Hughes Acidizing Hydrochloric acid 7647-01-0 15.00 0.19
Water 7732-18-5 85.00 1.11
Sand, White, 30/50 Baker Hughes Proppant Quartz 14808-60-7 100.00 6.34
mesh Hughes Proppant
Ferrotrol 300L Baker Hughes Iron Control Citric acid 77-92-9 60.00 0.00511000
Scaletrol 720 Baker Hughes Scale Inhibitor Ethylene glycol 107-21-1 30.00 0.00457000
Calcium chloride 10043-52-4 5.00 0.00076000
Alpha 1427 Baker Hughes Biocide Ethanol 64-17-5 5.00 0.00110000
Quaternary ammonium compounds,
benzyl-C12-16-alkyldimethyl, chlorides
68424-85-1 5.00 0.00110000
Glutaraldehyde 111-30-8 30.00 0.00659000
Didecyl dimethyl ammonium chloride 7173-51-5 10.00 0.00220000
FRW-18 Baker Hughes Friction Reducer Distillates, petroleum, hydrotreated light 64742-47-8 30.00 0.02
InFlo 250W Baker Hughes Surfactant Methanol 67-56-1 30.00 0.00068000
Surfactants 80.00 0.00180000
2-Butoxyethanol 111-76-2 5.00 0.00011000
Sand, White, 40/70 Baker Hughes Proppant Quartz 14808-60-7 100.00 4.66
Ingredients shown above are subject
to 29 CFR 1910.1200(i)
and appear on Material
Safety Data Sheets (MSDS). Ingredients shown below are Non-MSDS.
Water 7732-18-5 0.06
CI-14 Baker Hughes Corrosion Inhibitor Methanol 67-56-1 100.00 0.00196000
Alkenes, C>10 .alpha.- 64743-02-8 5.00 0.00010000
Propargyl alcohol 107-19-7 5.00 0.00010000
Fatty acids, tall-oil 61790-12-3 10.00 0.00020000
Ethoxylated C14-15 alcohols 68951-67-7 30.00 0.00059000
Ingredients shown above are subject
to 29 CFR 1910.1200(i)
and appear on Material
Safety Data Sheets (MSDS). Ingredients shown below are Non-MSDS.
Baker Hughes Surfactant Sorbitan Monooleate 0.00440315
Poly (acrylamide-co-acrylic acid) 0.02
Polyacrylate 0.00304414
Hydrochloric acid 7647-01-0
Potassium chloride 7447-40-7 0.00000761
Sodium chloride 7647-14-5 0.00000457
Ethoxylated Alcohol 0.00176126
Salt 0.00440315
Thiourea polymer 68527-49-1
Formalin 50-00-0
Water Operator Carrier Water 7732-18-5 100.00 86.63

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 CARRIZO (MARCELLUS) LLC 0.00 0 0.00 0 0.00 0
2011 CARRIZO (MARCELLUS) LLC 0.00 0 0.00 0 0.00 0
2012 CARRIZO (MARCELLUS) LLC 0.00 0 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 CARRIZO (MARCELLUS) LLC Drill Cuttings 1,184.00 Tons LANDFILL NY # 02S17
2010 CARRIZO (MARCELLUS) LLC Drill Cuttings 114.00 Tons LANDFILL NY31346244

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1985837 Primary Facility 2011-07-06 Drilling/Alteration No Violations Noted H&P 320 Comp. Man - Jeff Myers
1989472 Primary Facility 2011-07-19 Drilling/Alteration No Violations Noted Drillers log completed from 7230 - 11324'
2029523 Primary Facility 2011-12-27 Routine/Complete Inspection No Violations Noted
2103338 Primary Facility 2012-09-21 Routine/Complete Inspection Pending Water in cellar. Bubbles in cellar. Need to investigate further.
2104525 Primary Facility 2012-10-01 Follow-up Inspection Violation(s) Noted Met with Gary Byron, Tom Weller, Jesse Bonnice and water truck on site @ 10:30 AM to check for annular gas. Flooded cellar and saw bubbling. Tested w/ MSA Altair 5X multi-meter. Got reading of 25% LEL on combustibles.Slowly pumped water out of cellar to identify where bubbles are coming from. Gas is in 9 5/8" X 13 3/8" annulus.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2104525 650554 10/01/2012 2012-10-01 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days Administrative

For data sources see[8]

References