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37-129-25617

Well Details

Well ID: 37-129-25617
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Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: Loyalhanna Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: HARRY LYDIC 4A
License Status: ACTIVE
Spud Date:
Permit Date: 2005-01-13
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.461681
Longitude: -79.428656

For data sources see[1][2][3]

Well History

Date Event
2005-01-13 New Permit Application
2005-06-06 Drilling Completion
2005-06-06 Performed Spud Operation
2005-06-10 Drilling Completion
2005-06-16 Perforation
2009-08-04 NEWLY DRILLED
2009-08-04 SKIDDED RIG

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2005 PHILLIPS EXPLORATION INC 5532 100 0.00 0 0.00 0
2006 PHILLIPS EXPLORATION INC 13757.00 345 0.00 0 0.00 0
2007 PHILLIPS EXPLORATION INC 13961.00 365 0.00 0 0.00 0
2008 PHILLIPS EXPLORATION INC 9908.00 244 0.00 0 0.00 0
2009 PHILLIPS EXPLORATION INC 8993.00 365 0.00 0 0.00 0
2010 PHILLIPS EXPLORATION INC 9,369.00 320 0.00 0 0.00 0
2011 PHILLIPS EXPLORATION INC 7,453.00 256 0.00 0 0.00 0
2012 XTO ENERGY INC 7,868.00 366 0.00 0 0.00 0
2013 XTO ENERGY INC 5,678.00 365 0.00 0 0.00 0
2014 XTO ENERGY INC 5,698.00 365 0.00 0 0.00 0
2015 XTO ENERGY INC 5,129.20 365 0.00 0 0.00 0
2016 XTO ENERGY INC 4,625.00 366 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 3,608.00 334 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 4,361.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2013 XTO ENERGY INC Produced Fluid 44.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0020346
2016 XTO ENERGY INC Produced Fluid 8.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2016 XTO ENERGY INC Produced Fluid 8 Bbl CENT WASTE TRT FAC NPDES PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2733344 Primary Facility 2018-05-23 Routine/Complete Inspection No Violations Noted This well is tagged and in production. The well head casing, piping, equipment and grounded 100 bbl plastic fluid collection tank look ok.
2835067 Primary Facility 2019-02-04 Routine/Complete Inspection No Violations Noted This well is tagged and in production. The well head casing, piping, equipment and grounded 100 bbl plastic fluid collection tank look ok.

For data sources see[7]

References