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37-129-23060

Well Details

Well ID: 37-129-23060
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Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: Derry Township
Operator Name: FAIRMAN CORP
Well Pad ID:
Farm/Lease Name: MOLYNEAUX FARM
License Status: ACTIVE
Spud Date:
Permit Date: 1987-11-04
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.403467
Longitude: -79.3734

For data sources see[1][2][3]

Well History

Date Event
1987-11-04 New Permit Application
1987-11-24 Performed Spud Operation
1987-12-18 Drilling Completion
1987-12-18 Perforation
1987-12-18 Performed Stimulation
1988-05-31 NEWLY DRILLED
2016-07-11 Begin Plugging
2016-07-18 Finished Plugging
2019-08-26 Fully Plugged

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1987-12-18 sAND 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2001 HOME GAS & OIL CO INC 1591 365 0.00 0 0.00 0
2003 HOME GAS & OIL CO INC 1296 365 0.00 0 0.00 0
2010 FAIRMAN CORP 696.00 365 0.00 0 0.00 0
2011 FAIRMAN CORP 583.5 365 0.00 0 0.00 0
2012 FAIRMAN CORP 508.28 365 0.00 0 0.00 0
2013 FAIRMAN CORP 617.5 365 0.00 0 0.00 0
2014 FAIRMAN CORP 195.00 151 0.00 0 0.00 0
2015 FAIRMAN CORP 313.5 183 0.00 0 0.00 0
2016 FAIRMAN CORP 0.00 0 0.00 0 0.00 0
2017 FAIRMAN CORP 0.00 0 0.00 0 0.00 0
2018 FAIRMAN CORP 0.00 0 0.00 0 0.00 0

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2501162 Primary Facility 2016-07-12 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig crew was pumping second load of water down well bore loading it at the time of this inspection. All on site equipment looked ok.
2501178 Primary Facility 2016-07-12 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig crew pulling 1" string and setting plug from 3750' to 3150' at time of this inspection and planning to spot next plug to 2543' and third plug to 1884' and will then wash off. All equipment on site looked ok.
2501274 Primary Facility 2016-07-11 Plugging(Includes Plugged/Mined Through) No Violations Noted Inspection performed in response to the receipt of the Notice of Intention to Plug above referenced well. At the time of inspection well plugging ongoing. Site stable with no E& S issues in relation to site and/or access road.
2504893 Primary Facility 2016-07-21 Plugging(Includes Plugged/Mined Through) No Violations Noted At the time of inspection well appears to be plugged. Site stable with no E& S issues in relation to site and/or access road.
2596752 Primary Facility 2017-05-23 Site Restoration No Violations Noted At the time of inspection site restored. 70% vegetative cover established. No E&S issues.
751934 Primary Facility 1987-11-24 Drilling/Alteration No Violations Noted E&S,PITS OK
751935 Primary Facility 1988-05-03 Routine/Complete Inspection No Violations Noted E&S OK
751936 Primary Facility 1988-08-19 Routine/Complete Inspection No Violations Noted TANK; E&S OK

For data sources see[7]

References