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37-129-00546

Well Details

Well ID: 37-129-00546
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Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: Hempfield Township
Operator Name:
Well Pad ID:
Farm/Lease Name: PGH & BALTIMORE COAL JW454F
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: STORAGE WELL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.304261
Longitude: -79.645006

For data sources see[1][2][3]

Well History

Date Event
1917-04-20 Drilling Completion
1953-03-01 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2003 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2006 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2007 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2008 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2009 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2010 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2011 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2012 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2013 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2016568 Primary Facility 2011-11-03 Routine/Complete Inspection No Violations Noted FUTURE; SPEECH/TIONA; 0 PSIG; OPEN ANNULUS; NOT TIED IN
2196098 Primary Facility 2013-08-16 Plugging(Includes Plugged/Mined Through) No Violations Noted Rigged up to P&A on Wednesday, August 14. Baker Hughes ran collar log to find packer; 8/16/13- Baker Hughes on location to cut 3 1/2" casing above and below packer at 2595' and 2484' KB.
2201225 Primary Facility 2013-09-03 Plugging(Includes Plugged/Mined Through) No Violations Noted 3 1/2" casing all pulled from well including packer; Bond log run on 7" along with Gamma Ray, Neutron and caloper logs on open hole; Tripping back in hole to clean out hole and cement open hole with two cement plugs; cleaning out to attainable bottom/TD;
2204792 Primary Facility 2013-09-11 Plugging(Includes Plugged/Mined Through) No Violations Noted
2207825 Primary Facility 2013-09-26 Plugging(Includes Plugged/Mined Through) No Violations Noted Attempted to pull the 7" casing out of the hole after 3 cuts. Managed to remove 826' of casing.Cemented to top of 8 5/8". attempted to pull 8 5/8; perforated 700-710 and 542-552'; cemented with Class A Halvem with 180 sks thru 4 1/2" spotted at 758 ; Cement returns and cemented down down annulus of 10 3/4" casing to surface.; Well to be vent piped; plugging complete.
2222958 Primary Facility 2013-11-18 Site Restoration No Violations Noted Certificate of Plugging received by the Department on 11/6/2013. At the time of inspection the well appeared to be plugged. The site has been temporary stabilized. The site does not meet the restoration criteria of 70% vegetative coverage. A follow up inspection will be conducted in the spring of 2014 to ensure the restoration criteria is met.

For data sources see[6]

References