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37-125-01603

Well Details

Well ID: 37-125-01603
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Country: United States
State: Pennsylvania
County: Washington
Municipality: Carroll Township
Operator Name: DEVELOPED RESOURCES INC
Well Pad ID:
Farm/Lease Name: PITTSBURGH CONSOL COAL 2
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.214250
Longitude: -79.9695

For data sources see[1][2][3]

Well History

Date Event
1925-01-01 Drilling Completion
1987-11-02 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 AGOSTONI JOSEPH 3.00 365 0.00 0 0.00 0
2000 DEVELOPED RESOURCES INC 1924 365 0.00 0 0.00 0
2001 DEVELOPED RESOURCES INC 1800 365 0.00 0 0.00 0
2002 DEVELOPED RESOURCES INC 1424 365 0.00 0 0.00 0
2003 DEVELOPED RESOURCES INC 1020 365 0.00 0 0.00 0
2004 DEVELOPED RESOURCES INC 900 365 0.00 0 0.00 0
2015 DEVELOPED RESOURCES INC 3,600.00 365 0.00 0 0.00 0
2016 DEVELOPED RESOURCES INC 2,608.00 365 0.00 0 0.00 0
2017 DEVELOPED RESOURCES INC 2,025.00 365 0.00 0 0.00 0
2018 DEVELOPED RESOURCES INC 1,619.00 365 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2346422 Primary Facility 2015-02-25 Follow-up Inspection No Violations Noted Follow–up to stray gas issues at residence 286 Courtney Hill Rd. The operator is sampling well (125-01603) as Department Regulations require. Waiting on sample results in near future. We walked the area of People Gas Line to discover a line leak.
2369734 Primary Facility 2015-05-04 Drilling/Alteration No Violations Noted Follow–up to requirements set up by ( Depatrment ). Test the outside of Prod. Casing with 3- holes 24" deep ( No Pressure).Rock pressure in 24 Hrs. period is 88 psi. Pressure test flow from well to meter station @ 25 psi for 30 min. NO LINE LOSS.

For data sources see[6]

References