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37-125-01003

Well Details

Well ID: 37-125-01003
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Country: United States
State: Pennsylvania
County: Washington
Municipality: Cecil Township
Operator Name: ALL AMER ENERGY INC
Well Pad ID:
Farm/Lease Name: WALLACE & MILLER 6
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: COMB. OIL&GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.363444
Longitude: -80.2235

For data sources see[1][2][3]

Well History

Date Event
1901-01-01 Drilling Completion
1986-04-17 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2000 ALL AMER ENERGY INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2598534 Primary Facility 2015-12-17 Routine/Complete Inspection No Viols - Permanently Shut Down Visited site w/ (RETTEW) representative as part of the Southern Beltway Project. Wellhead is intact w/ 4 1/2" casing on casing clamp, tubinghead and 2 1/2" tubing & rods. May still be producing gas, but has not pumped oil for many years. Metal structures of old enginehouse, pumphouse, walking beam and derrick (collapsed) are present, but very little of the wooden structures remain, except the large beams. Location is benched area on wooded slope near access road.
2598550 Primary Facility 2017-04-18 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule
2598566 Primary Facility 2017-05-08 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost pulled all rods & tubing.TIMCO logging hole, can't log below 1500 feet, due to bridge. Logged from bridge to surface; Bottom 4" casing @ 1295 feet, with holes or partings @ 870 feet &780 feet. Tight spots indicated on bond log, so will be perfing casing.
2598598 Primary Facility 2017-05-09 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost got cement string through the bridge @1500 feet to 2427 feet, stopping one joint off of TD of ~2450 feet. Pumped 100 sack bottom-hole plug.
2598618 Primary Facility 2017-05-11 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost tagged TOC plug @ ~940 feet. TIMCO TIH, perfed @940', 900', 850' & 800'. Yost pulled on 4" casing pulled free (parted @ 870 & 780 feet).
2598630 Primary Facility 2017-05-16 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost pulled 842 feet of 4" casing. TIMCO TIH to log 6 5/8" casing, set down @ 642, logged to surface. Yost TIH w/ string of tools and knocked out btidge. Loggers got to below 800 feet, perfed every 50 feet from 800'-100'.
750832 Primary Facility 1987-06-10 Routine/Complete Inspection No Violations Noted NOT OPERATING
965072 Primary Facility 2000-09-11 Routine/Complete Inspection Violation(s) Noted Abandoned & unplugged. Standard derrick standing, collapsed shed, nearly all original equipment here in state of abandonment. No access, completely forested perimeter. Hillside. Walking beam era.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
965072 250569 09/11/2000 2000-09-11 210UNPLUG - Failure to plug a well upon abandonment Administrative Company is bankrupt.

For data sources see[6]

References