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37-115-21430

Well Details

Well ID: 37-115-21430
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Country: United States
State: Pennsylvania
County: Susquehanna
Municipality: Choconut Township
Operator Name: REPSOL OIL & GAS USA LLC
Well Pad ID: 150176
Farm/Lease Name: TRAVER 07 081 07 E 7H
License Status:
Spud Date:
Permit Date: 2013-08-14
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.953133
Longitude: -76.020814

For data sources see[1][2][3]

Well History

Date Event
2013-08-14 New Permit Application
2013-11-15 Performed Spud Operation
2014-04-13 Drilling Completion
2014-05-29 Perforation
2014-06-08 Performed Stimulation
2015-01-12 DEVIATED

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2014-06-21 2014-06-21 5,907 5,940,580 28,000

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 Water Customer Carrier Water 7732-18-5 100 79.2982 49,576,500.0
AQUCAR DB 5 (Water Treatment Microbiocide) Trican Biocide 2,2-dibromo-3-nitrilopropionamide 10222-01-2 5 0.001343 839.429
Polyethylene glycol 25322-68-3 65.2 0.017509 10946.2
Sodium Bromide 7647-15-6 1.5 0.000403 251.829
Dibromoacetonitrile 3252-43-5 0.5 0.000134 83.9429
LSI-21 (Scale Inhibitor) Trican Scale Inhibitor Acrylic Polymer 28205-96-1 15 0.003835 2397.38
Sodium Salt of Phosphate Ester 68131-72-6 15 0.003835 2397.38
100 Mesh, Bulk (over 20K lbs)* Trican Proppant Crystalline silica: Quartz (SiO2) 14808-60-7 100 7.1073 4,443,420.0
FR-8 Trican Friction Reducer Petroleum distillates, dewaxed heavy paraffinic 64742-65-0 8 0.00528 3301.09
Mineral oil/ light hydrotreated pet. distillate 64742-47-8 28 0.01848 11553.8
Ammonium Chloride 12125-02-9 1.5 0.00099 618.954
Petroleum distillates, hydrotreated heavy paraffinic 64742-54-7 8 0.00528 3301.09
AI-7NR (Acid Inhibitor) Trican Acid Inhibitor Prop-2-yn-1-ol 107-19-7 1 0.00001000 6.1756
15% HCL Customer Carrier Hydrochloric acid 7647-01-0 15 0.002142 1339.44
White 40/70 Trican Proppant Crystalline silica: Quartz (SiO2) 14808-60-7 100 8.13657 5,086,910.0
7 1/2% HCL Trican Carrier Hydrochloric acid 7647-01-0 7.5 0.00623 3894.76
3 1/2% HCL Trican Carrier Hydrochloric acid 7647-01-0 3.5 0.009811 6133.87
Other Chemicals Alkyloxypolyethylene oxyethanol 84133-50-6 0 0 0
Water 7732-18-5 0 0 0
Nonionic Surfactant Proprietary 0 0 0
Acrylamide 79-06-1 0 0 0
Trade Secret Proprietary 0 0 0
Sorbitan monooleate 1338-43-8 0 0 0
Acrylamide P/W acrylic acid ammonium salt 26100-47-0 0 0 0
Polyethylene glycol monooleate 9004-96-0 0 0 0
Ammonium Acrylate 10604-69-0 0 0 0
Anionic polyacrylamide copolymer Proprietary 0 0 0
Sorbitol Tetraoleate 61723-83-9 0 0 0
Isopropanol 67-63-0 0 0 0
White 30/50 Trican Proppant Crystalline silica: Quartz (SiO2) 14808-60-7 100 4.95855 3,100,040.0
FEAC-20 (Iron Control) Trican Iron Control Acetic acid 64-19-7 45 0.001049 655.849
Citric acid 77-92-9 30 0.000699 437.232

For data sources see[5]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
2014-06-08 0 0 0

For data sources see[6]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2013 REPSOL OIL & GAS USA LLC 0.00 0 0.00 0 0.00 0
2014 REPSOL OIL & GAS USA LLC 0.00 0 0.00 0 0.00 0
2015 REPSOL OIL & GAS USA LLC 265,725.10 48 0.00 0 0.00 0
2016 REPSOL OIL & GAS USA LLC 1,545,543.50 365 0.00 0 0.00 0
2017 REPSOL OIL & GAS USA LLC 1,076,451.70 365 0.00 0 0.00 0
2018 REPSOL OIL & GAS USA LLC 718,933.30 365 0.00 0 0.00 0
2019 REPSOL OIL & GAS USA LLC 602,116.10 364 0.00 0 0.00 0

For data sources see[7]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2013 REPSOL OIL & GAS USA LLC Drill Cuttings 12.58 Tons LANDFILL 8-0728-0004/013
2014 REPSOL OIL & GAS USA LLC Fracing Fluid Waste 20,559.90 Bbl REUSE OTHER THAN ROAD SPREADING
2014 REPSOL OIL & GAS USA LLC Drill Cuttings 1,012.89 Tons LANDFILL 8-0728-0004/013
2015 REPSOL OIL & GAS USA LLC Produced Fluid 1,975.43 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123
2015 REPSOL OIL & GAS USA LLC Produced Fluid 2,944.59 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC010
2016 REPSOL OIL & GAS USA LLC Produced Fluid 187.93 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123
2016 REPSOL OIL & GAS USA LLC Produced Fluid 10,679.30 Bbl REUSE OTHER THAN ROAD SPREADING
2016 REPSOL OIL & GAS USA LLC Produced Fluid 1,235.20 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC010
2016 REPSOL OIL & GAS USA LLC Produced Fluid 1,006.35 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2017 REPSOL OIL & GAS USA LLC Other Oil & Gas Wastes 195.00 Bbl REUSE (AT WELL PAD)
2017 REPSOL OIL & GAS USA LLC Produced Fluid 598.59 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2017 REPSOL OIL & GAS USA LLC Produced Fluid 4,950.64 Bbl REUSE (AT WELL PAD)
2018 REPSOL OIL & GAS USA LLC Produced Fluid 397.37 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2018 REPSOL OIL & GAS USA LLC Produced Fluid 2,642.43 Bbl REUSE (AT WELL PAD)
2019 REPSOL OIL & GAS USA LLC Produced Fluid 365.15 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2019 REPSOL OIL & GAS USA LLC Produced Fluid 1,735.04 Bbl REUSE (AT WELL PAD)
2019 REPSOL OIL & GAS USA LLC Produced Fluid 28.25 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123

For data sources see[8]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2219099 Primary Facility 2013-11-05 Preoperation Inspection No Violations Noted
2244902 Primary Facility 2014-02-11 Routine/Complete Inspection No Violations Noted Condcutor set
2264798 Primary Facility 2014-04-08 Drilling/Alteration No Violations Noted Currently at 6124'
2291449 Primary Facility 2014-07-31 Incident- Response to Accident or Event No Violations Noted Arrived at the site at 12:25 in response to a spill of (2) barrels of flowback fluid contained on the well pad. I was accompanied by Matt Shope, DEP O&G WQS during the inspection. Steve Jorgenson, site Company Man of Talisman Energy, who was on the location when the spill occurred, contacted the Department at 8:55 AM on 7/31/14 to report the spill incident. Mr. Jorgenson reported that the spill occurred at 3:55 AM on 7/3/1/14.
2321235 Primary Facility 2014-10-27 Incident- Response to Accident or Event No Violations Noted Arrived at the site at 12:25 in response to a spill of (4) gallons of diesel fuel. There was no activity at the site during the inspection. I was accompanied by Frank Hoehle, DEP O&G WQS, during the inspection. Upon arriving to the location we observed (2) overpack drums, (1) (95) gallons in capacity, the other (65) gallons in capacity. We suspected that the drums contained impacted pad surface material assocaited with the diesel fuel release. We walked the pad surface area in and effort to locate the area where the release occurred. We noticed a small area of dark staining of the pad surface in the eastern section of the Pad at N-41°57’14” W-76°01 13”. The pad surface material had a petroleum/diesel fuel to it. Based on our observations and the odor of the pad surface material where the staining was observed, we concluded that the diesel fuel released to the pad surface had not been compleltely remediated.
2375280 Primary Facility 2015-06-01 Routine/Complete Inspection No Violations Noted The Department was on site to conduct a routine complete inspection of the Traver well site.
2386258 Primary Facility 2015-07-09 Routine/Complete Inspection No Violations Noted
2498592 Primary Facility 2016-07-01 Routine/Complete Inspection No Violations Noted At time of inspection, arrived on site at 13:00p.m., the cellar was full of water with no bubbling noticed, the (20x13) vent pipe was open and venting into the atmosphere with no gas detected, the (13x9) vent pipe was open and venting into the atmosphere with no gas detected, the (9x5) vent pipe was open and venting into the atmosphere with no gas detected. There was 846psi on the production casing and 464psi on the production tubing. I took a walk around the location and noticed that the man hole on one of the production water tanks was leaking. I contacted Talisman Energy and spoke with Lance Rydle, I told him of the man hole cover and he told me that he would get it taken care of. There was no production water outside of the containment.

I left the site at 13:35p.m.

2588484 Primary Facility 2017-04-27 Routine/Complete Inspection No Violations Noted At time of inspection, arrived on site at 11:30a.m.

The cellar was full of water with no bubbling noticed. The (20x13) annulus vent pipe was open and venting into the atmosphere with no gas detected, the (13x9) annulus vent pipe was open and venting into the atmosphere with no gas detected, the (9x5) annulus vent pipe was open and venting into the atmosphere with no gas detected. There was 603psi on the production casing and 402psi on the production line. I took a walk around the location and there were no obvious concerns noticed. I left the site at 12:10p.m.

2697772 Primary Facility 2018-02-16 Routine/Complete Inspection No Violations Noted At time of inspection.

The well was in production. The cellar was about half full of water and ice with no bubbling noticed. The (20x13), (13x9) and (9x5) annuli were venting into the atmosphere and there was no gas detected. I took a walk around the location and there were no obvious concerns noticed. There were no violations noted.

2740461 Primary Facility 2018-06-08 Routine/Complete Inspection No Violations Noted I performed a RTNC inspection of the Traver pad. The wells associated with this pad are the 115-21429 and the 115-21430. These wells were properly labeled. The access road and pad surface were stable and solid. The vegetation surrounding the pad was lush and healthy and there were no erosional issues noted.

There were no violations noted.

2767469 Primary Facility 2018-08-23 Routine/Complete Inspection No Violations Noted I performed a Routine Complete Inspection of the Traver well pad. The wells associated with this pad are the 115-21429 and the 115-21430. The wells were properly labeled.

The township and state roads in the area, as well as all the creeks and waters had recently been hit hard by very heavy, sustained rainfall and many roads had been closed or under repair. The well pad access road and pad surface was unaffected however and there was no erosion noted.

The containment surrounding the well pad structures had some water in it but it was not excessive. There had been local rainfall as recently as last night. The containment all looked competent.

The well cellars had water but there was no bubbling present.

The cut and fill slopes as well as the topsoil pile all had adequate vegetation. There was healthy, perennial growth on all vegetated surfaces as well as some woody plant growth. No erosional forces appeared to be affecting the slopes at the time of inspection.

There were no erosional issues present

2794706 Primary Facility 2018-10-25 Routine/Complete Inspection No Violations Noted At time of inspection.

The well was in production. There was water 3' below grade in the cellar and there was no bubbling noticed. There was a methanol tank and pump (see photo) in containment and the containment appeared to be in good condition. I took a walk around the location and there were no obvious concerns noticed. There were no violations noted.

For data sources see[9]

References