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37-115-20833

Well Details

Well ID: 37-115-20833
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Country: United States
State: Pennsylvania
County: Susquehanna
Municipality: Harford Township
Operator Name: CABOT OIL & GAS CORP
Well Pad ID:
Farm/Lease Name: R CAREY 4
License Status:
Spud Date:
Permit Date: 2012-01-19
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.75
Longitude: -75.689917

For data sources see[1][2][3]

Well History

Date Event
2012-01-19 New Permit Application

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2012 CABOT OIL & GAS CORP 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2354801 Primary Facility 2015-03-25 Routine/Complete Inspection No Violations Noted The Department was on site to conduct a routine complete inspection on the R. Carey well pad. Permits associated with this site are:
2530765 Primary Facility 2016-10-21 Routine/Complete Inspection No Violations Noted On 10/21/16, the Department conducted an inspection of the COG Carey R. Pad located in Harford Township, Susquehanna County. 3 Wells have been drilled on this pad and appear to be in production, the 1H(115-20836), the 2H(115-20835), and the 3H(115-20834). The 4H(115-20833) was proposed but never built. The well pad and adjoining tank pad have good stabilization. There were 2 standing water puddles located on the well pad. Both puddles were tested with an Extech Exstik II Conductivity Meter. Both revealed measurements of 200 microsiemens. Next, the conductivity of the standing water within the production tank containment was measured and found to be at 600 microsiemens. There was approximately 3” of water in this containment. A Time Extension Request has been granted for the ESCGP for this site by the Department and will be effective until September 30, 2017. No violations noted.

For data sources see[6]

References