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37-085-23610

Well Details

Well ID: 37-085-23610
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Country: United States
State: Pennsylvania
County: Mercer
Municipality: Coolspring Township
Operator Name: BOBCAT WELL & PIPELINE LLC
Well Pad ID:
Farm/Lease Name: MIKLOS UNIT 1
License Status: ACTIVE
Spud Date:
Permit Date: 2004-07-20
Well Type: COMB. OIL&GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 41.261968
Longitude: -80.248587

For data sources see[1][2][3]

Well History

Date Event
2004-07-20 New Permit Application
2004-10-11 Performed Spud Operation
2004-10-17 Drilling Completion
2004-10-25 Perforation
2005-04-12 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2005 D & L ENERGY INC 11738 324 0.00 0 0.00 0
2008 D & L ENERGY INC 9440.00 366 0.00 0 0.00 0
2010 D & L ENERGY INC 6,616.00 365 0.00 0 0.00 0
2011 D & L ENERGY INC 6,417.00 365 0.00 0 0.00 0
2012 D & L ENERGY INC 6,279.00 365 0.00 0 0.00 0
2013 D & L ENERGY INC 6,047.00 365 0.01 365 0.00 0
2015 BOBCAT WELL & PIPELINE LLC 4,391.00 365 0.00 0 0.00 0
2016 BOBCAT WELL & PIPELINE LLC 2,064.00 243 0.00 0 0.00 0
2017 BOBCAT WELL & PIPELINE LLC 3,736.00 357 0.00 0 0.00 0
2018 BOBCAT WELL & PIPELINE LLC 5,754.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2005 D & L ENERGY INC Brine 970.00 Bbl Injection Disposal Well
2010 D & L ENERGY INC Produced Fluid 95.00 Bbl Injection Disposal Well 34-155-23584
2010 D & L ENERGY INC Produced Fluid 30.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 34-007-22038
2011 D & L ENERGY INC Produced Fluid 68.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 34-099-23127
2012 D & L ENERGY INC Produced Fluid 79.00 Bbl Injection Disposal Well 34-007-20919
2013 D & L ENERGY INC Produced Fluid 53.00 Bbl Injection Disposal Well 34-007-20919
2016 BOBCAT WELL & PIPELINE LLC Produced Fluid 19.00 Bbl Injection Disposal Well 34-155-24063
2017 BOBCAT WELL & PIPELINE LLC Produced Fluid 23.00 Bbl ROAD SPREADING
2018 BOBCAT WELL & PIPELINE LLC Produced Fluid 128.00 Bbl Injection Disposal Well 34-007-21847

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1384767 Primary Facility 2004-10-12 Drilling/Alteration No Violations Noted
1390308 Primary Facility 2004-10-19 Drilling/Alteration No Violations Noted
1399726 Primary Facility 2004-12-06 Administrative/File Review No Violations Noted Well record review
2682056 Primary Facility 2018-01-12 Complaint Inspection No Violations Noted GPS coordinates taken at well with inspection app. Well is approximately 979 ft east from tank battery. Tubing is open to sales. Production casing is open to a domestic gas meter. Surface casing is open to the tank. The original complaint 12/2/17 stated that the well was leaking. Emergency Response report stated that the domestic gas regulator which is the responsibility of the gas user to repair was leaking. Operator was contacted and stated that gas user was responsible for repairs but if the Department wanted the leak shut off that they would shut the valve stopping the leak and user from getting gas for heat. Complaint received again 1/11/18 that regulator still leaking. Upon inspection of well did not see any leaks. Did see foot prints in mud and someone wrote on regulator good. Will contact complainant. - Invalid Complaint Id. - 331208

For data sources see[7]

References