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37-081-21683

Well Details

Well ID: 37-081-21683
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Country: United States
State: Pennsylvania
County: Lycoming
Municipality: Gamble Township
Operator Name: SENECA RESOURCES CO LLC
Well Pad ID: 153513
Farm/Lease Name: EASTON 101H 52655
License Status:
Spud Date: 2017-07-25
Permit Date: 2017-05-24
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 41.367711
Longitude: -76.994264

For data sources see[1][2][3]

Well History

Date Event
Deviated
2017-05-24 New Permit Application
2017-07-25 Performed Spud Operation
2017-09-13 Drilling Completion
2017-10-30 MOD

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2017-11-10 2017-11-30 9,152 8,303,020 0

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 KFEAC-30 Keane Iron Control Acetic acid 64-19-7 60 0.000608981 480.245
Citric acid 77-92-9 40 0.000405988 320.164
KFR-20 Keane Friction Reducer cololymer of 2-propenamide 69418-26-4 30 0.0278845 21989.8
Alcohols, C12-16, ethoxylated 68551-12-2 2 0.00185897 1465.99
Water 7732-18-5 45 0.0418267 32984.8
Mineral oil/ light hydrotreated pet. distillate 64742-47-8 20 0.0185897 14659.9
Ammonium Chloride 12125-02-9 1 0.000929483 732.995
oleic acid diethanolamide 93-83-4 2 0.00185897 1465.99
DustProof (Proppant) Keane Proppant Crystalline silica: Quartz (SiO2) 14808-60-7 99.9 11.6969 9,224,250.0
Blend Proprietary 0.1 0.0117086 9233.48
MBC-516 Keane Biocide Didecyl dimethyl ammonium chloride 7173-51-5 8 0.000714641 563.57
ethanol 64-17-5 2.8 0.000251066 197.992
gluteral 111-30-8 26.7 0.00239409 1887.99
quaternary ammonium compounds,
benzyl-C12-16-alkyldimethyl, chlorides
68424-85-1 5.3 0.000476129 375.477
KAI-12 Keane Acid Inhibitor propan-2-ol 67-63-0 5 0.00006012 47.409
alcohols, c7-9-0so, c8-rich 68526-83-0 5 0.00006012 47.409
fatty imidazoline 61790-69-0 5 0.00006012 47.409
prop-2-yn-1-0l 107-19-7 5 0.00006012 47.409
xylne 1330-20-7 5 0.00006012 47.409
ethylbenzene 100-41-4 1 0.00001202 9.482
methanol 67-56-1 90 0.00108211 853.36
KSI-19 NW Keane Scale Inhibitor Aqueous Solution Proprietary 100 0.00101111 797.365
7.5% Acid Keane Acidizing Hydrochloric Acid 7647-01-0 7.5 0.0351561 27724.3
Water 7732-18-5 92.5 0.433592 341933
Water (Clean - Acid - Chems) Seneca Resources Carrier/Base Fluid Water 7732-18-5 100 87.7045 69,164,200.0
KSI-19 Keane Scale Inhibitor Aqueous Solution Proprietary 100 0.0129777 10234.3

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2017 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2018 SENECA RESOURCES CO LLC 1,602,779.98 290 0.00 0 0.00 0
2019 SENECA RESOURCES CO LLC 1,081,086.00 359 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2017 SENECA RESOURCES CO LLC Produced Fluid 1,480.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2017 SENECA RESOURCES CO LLC Synthetic Liner Materials 9.13 Tons LANDFILL 301358
2017 SENECA RESOURCES CO LLC Produced Fluid 107.14 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005
2017 SENECA RESOURCES CO LLC Produced Fluid 171.43 Bbl REUSE (AT WELL PAD)
2017 SENECA RESOURCES CO LLC Drill Cuttings 1,632.13 Tons LANDFILL 301358
2017 SENECA RESOURCES CO LLC Waste Water Treatment Sludge 30.68 Tons RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005
2018 SENECA RESOURCES CO LLC Waste Water Treatment Sludge 128.43 Tons RESIDUAL WASTE PROCESSING FACILITY WMGR123
2018 SENECA RESOURCES CO LLC Other Oil & Gas Wastes 39.28 Bbl REUSE (AT WELL PAD)
2018 SENECA RESOURCES CO LLC Produced Fluid 2,520.71 Bbl REUSE (AT WELL PAD)
2018 SENECA RESOURCES CO LLC Produced Fluid 12,879.56 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2018 SENECA RESOURCES CO LLC Drill Cuttings 1.50 Tons LANDFILL 301358
2018 SENECA RESOURCES CO LLC Produced Fluid 105.24 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005
2018 SENECA RESOURCES CO LLC Synthetic Liner Materials 7.98 Tons LANDFILL 301358
2018 SENECA RESOURCES CO LLC Other Oil & Gas Wastes 82.86 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2019 SENECA RESOURCES CO LLC Other Oil & Gas Wastes 18.57 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005
2019 SENECA RESOURCES CO LLC Produced Fluid 814.99 Bbl REUSE (AT WELL PAD)
2019 SENECA RESOURCES CO LLC Produced Fluid 74.29 Bbl STORAGE PENDING DISPOSAL OR REUSE WMGR123NC038
2019 SENECA RESOURCES CO LLC Produced Fluid 2,355.72 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2019 SENECA RESOURCES CO LLC Produced Fluid 1,063.00 Bbl RESIDUAL WASTE TRANSFER FACILITY WMGR123NC039
2019 SENECA RESOURCES CO LLC Produced Fluid 102.85 Bbl INJECTION DISPOSAL WELL 34-155-24079
2019 SENECA RESOURCES CO LLC Other Oil & Gas Wastes 18.57 Bbl RESIDUAL WASTE TRANSFER FACILITY WMGR123NC039
2019 SENECA RESOURCES CO LLC Synthetic Liner Materials 2.22 Tons LANDFILL 301358
2019 SENECA RESOURCES CO LLC Produced Fluid 310.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC003

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2601629 Primary Facility 2017-06-01 Drilling/Alteration No Violations Noted Weather: Sunny. Arrived @ 08:00. Patterson 339 on location, 9-5/8” cement job recently completed. At the time of my inspection, crew were nippling up BOPs. Met with company man Danny Berrera and drilling and construction foreman Scott Barr who was onsite to supervise spudding of up to 3 conductors for the Easton 102H, 103H, and101H. Also onsite was an Express Energy Services auger rig. Plan was to set these conductors deeper (formerly 77’, increased to 120’-150’) because the 31H had lost circulation high up in the hole (90-100’ from surface). For 31H, had pumped extra cement in this shallow section before proceeding further. Left location @ 09:00.
2606270 Primary Facility 2017-06-15 Routine/Complete Inspection No Violations Noted Routine complete inspection; 6/15/1017. The Patterson rig 339 was on the Easton 30H (081-21634) running 9 5/8" intermediate casing in the hole. I walked the site with Justin Greene (company man). The containment looked excellent, clean, and well maintained. Cuttings management looks clean and well kept. Chemical storage was all on containment and clearly separated. Overall, the site looks very good. No violations noted.
2645929 Primary Facility 2017-10-11 Drilling/Alteration No Violations Noted Arrived at 11:00. Weather: warm, rain. Met with company man Anthony Murphy. Keane Frac onsite fraccing the 102H and 103H wells. At the time of my inspection, stage 6 on the 103H, had been perf'ed, gun was stuck at 14,477. Left at 12:20. No violations were noted during this inspection.
2650628 Primary Facility 2017-10-16 Routine/Complete Inspection No Violations Noted I entered the site and met with Anthony Murphy (Company Man). At the time of the inspection, the wireline was running in the Easton 102H (081-21684) on the 13th stage while the 12th stage was under pressure on the Easton 103H(081-21682). Field conductivity in puddles adjacent to the produced water storage containment was between 267-588 umhos/cm. Field conductivity in containment at the southeastern corner of containment was 356 umhos/cm. Dust was visible coming from the sand handling equipment. After looking into the sand concern, the filters were being cleaned before I left the site. The site was in excellent condition and as usual, the containment is graded toward the cellars and covered with rig mats. No violations noted.
2650651 Primary Facility 2017-10-20 Drilling/Alteration No Violations Noted Arrived at 14:40. Met with Anthony Murphy, company man, and Mike Cauley, frac engineer. At the time of my inspection, they were preparing to frac stage 18 on the 102H and 103H. They were also then going to frac stage 3 on the 29H. No violations were obaerved at the time of my inspection.
2654841 Primary Facility 2017-10-27 Routine/Complete Inspection No Violations Noted I met Justin Weaver when I arrived on-site. Frac was idle, and Justin informed me that they are only fracing at night. Individual secondary containments were in good condition, and rig mats on sitewide containment were clean and dry. Water trucks were offloading to the reused water tanks. Justin estimated that the frac would continue through the end of November.
2672657 Primary Facility 2017-12-19 Drilling/Alteration No Violations Noted Arrived at 11:50. Weather sunny, windy, temps in 40s. M35 with Anthony Murphy, company man Seneca. Currently drilling out plugs. Running 2 snubbing rigs (Hydraulic Pressure Control). At the time of my inspection, had just finished a well, changed out the bag, and were moving to the final well. No violations observed at the time of my inspection.
2676391 Primary Facility 2017-12-19 Site Restoration No Violations Noted The operator submitted a Post Drilling Well Site Restoration Report on 11/10/2017. Post Construction Stormwater Management (PCSM) plans have been implemented but vegetation is not sufficient to be considered permanently stabilized. Pipeline construction operations were ongoing at the time of the inspection.

After entering the site, I met with Anthony Murphy and we walked the site. One snubbing unit/workover rig was on the Easton 29H (081-21633) while the second was on the 101H (081-21683). The site was very clean and housekeeping was excellent. Individual containments were well placed and effective. Production equipment and flow lines were being installed as the site transitions toward flow-back/production. Overall, the site is in excellent condition but does not meet the requirements to be considered restored. No violations noted.

2682045 Primary Facility 2018-01-11 Drilling/Alteration No Violations Noted Arrived at 11:00. Met with Lee Kennemoth, completions foreman. Flow back operations are nearing a conclusion with 6 of the 7 wells on the pad are flowing gas to pipeline. Flow back ops anticipate another few days before turning site over to production. For the 101H, plugs still need to be drilled out.
2715436 Primary Facility 2018-04-04 Routine/Complete Inspection No Violations Noted Routine Inspection; 4/4/2018.

I met Aaron Hoffman (company man),and walked the site. At the time of the inspection, the wells were on temporary sand separation and produced water was being transferred from the production tanks to a battery of frac-tanks. Water on the well pad surface had field conductivity between 350-545 umhos/cm. Field conductivity at the south end of the frac-tank battery containment was 5,350 umhos/cm. I recommended (to Mr. Hoffman) that the frac-tank battery containment be vacuumed as soon as it is practical. The vac-truck was removing water from the well cellars and surrounding containment during the inspection. Water was ponded near the entrance to the site west of SugarCamp Road. I recommend evaluating the drainage in this existing swale between the two houses. No violations noted.

2746600 Primary Facility 2018-06-27 Site Restoration No Violations Noted Well Site Restoration Report Inspection; 6/27/2018.

At the time of the inspection the wells were in production and produced water was being stored in frac tanks on containment (a pump was installed and was actively pumping from the permanent production tanks to the frac tanks. HRI was onsite removing a temporary HDPE water line which had previously been buried in the pad. I recommend restoring the site in accordance with the ESCGP or requesting a 2-year extension. I recommend denying the Well Site Restoration Report. No violations noted.

2819098 Primary Facility 2018-12-26 Routine/Complete Inspection No Violations Noted Seven wells staged for production. Seven GPUs within 10 inch containment. No leaks detected from production equipment.

Service rig on location to run additional production pipe. Containment and rig matting in place. All baker tanks within containment. No violations noted.

For data sources see[8]

References