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37-081-21242

Well Details

Well ID: 37-081-21242
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Country: United States
State: Pennsylvania
County: Lycoming
Municipality: Anthony Township
Operator Name: RANGE RESOURCES APPALACHIA LLC
Well Pad ID:
Farm/Lease Name: CORSON UNIT 4H
License Status:
Spud Date:
Permit Date: 2013-07-01
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.314356
Longitude: -77.189453

For data sources see[1][2][3]

Well History

Date Event
2013-07-01 New Permit Application
2014-05-27 Permit Renewal Application

For data sources see[4]



Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2315253 Primary Facility 2014-10-15 Incident- Response to Accident or Event No Violations Noted Operator reported 6-8 barrels of diesel-based drill mud released to the pad surface. Due to intense rain, the product was mobilized from the pad, down a rock-lined swale, and into a sedimentation basin. booms and pads were installed but evidence of the spill was noted throughout. Violations noted to the active 2H well (081-21050).
2315271 Primary Facility 2014-10-16 Incident- Response to Accident or Event No Violations Noted The plan going forward was to continue to vacuum from the sump on the well pad, install temporary outlets for stormwater to divert water away from the spill area, and begin excavating the rock-lined swale based on PID field screening. After the rock-lined swale is excavated, install tremporary E&S measures to minimize accelerated erosion and wait (hopefully no more than 3-5 days) for tanks and containment to be removed from overtop the original spill area. After the containment is removed the final excavation and confirmation sampling can begin.
2369191 Primary Facility 2015-05-11 Incident- Response to Accident or Event No Violations Noted At 16:28, I met with Zachary Subra on the location. On 5/9/2015, Range Resources reported 35-40 gallons of reclaimed produced water/brine was release to the pad surface. The release was then cleaned-up the same day and staged on containment. At the time of the inspection, trucks and equipment were being staged on the location in support of the completions operations on the nearby Roupp pad. A small 20'X20' area had been scraped near the southwest corner of the well pad. Due to the extremely dry conditions I screened field conductivity by using Deionized water mixed with the sample material. Field conductivity using this leachate test was 690 umhos/cm in the excavated area. Based on the field investigation, the release estimate appears reasonable. Violations Noted and Immediately Corrected.

For data sources see[5]

References