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37-065-26146

Well Details

Well ID: 37-065-26146
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Country: United States
State: Pennsylvania
County: Jefferson
Municipality: Winslow Township
Operator Name: FARRINGTON & HEPLER GAS & OIL INC
Well Pad ID:
Farm/Lease Name: SHUTTLEWORTH 4
License Status:
Spud Date:
Permit Date: 2008-01-24
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.108306
Longitude: -78.907919

For data sources see[1][2][3]

Well History

Date Event
2008-01-24 New Permit Application
2008-03-24 Performed Spud Operation
2008-04-04 Drilling Completion
2008-11-05 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2011 FARRINGTON & HEPLER GAS & OIL INC 445.63 365 0.00 0 0.00 0
2012 FARRINGTON & HEPLER GAS & OIL INC 180.11 365 0.00 0 0.00 0
2013 FARRINGTON & HEPLER GAS & OIL INC 134.86 365 0.00 0 0.00 0
2014 FARRINGTON & HEPLER GAS & OIL INC 0.43 365 0.00 0 0.00 0
2015 FARRINGTON & HEPLER GAS & OIL INC 6.9 365 0.00 0 0.00 0
2018 FARRINGTON & HEPLER GAS & OIL INC 16.79 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2011 FARRINGTON & HEPLER GAS & OIL INC Produced Fluid 8.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1699640 Primary Facility 2008-04-16 Drilling/Alteration No Violations Noted
1702909 Primary Facility 2008-04-30 Routine/Complete Inspection No Violations Noted
1730890 Primary Facility 2008-08-26 Routine/Complete Inspection No Violations Noted
1734558 Primary Facility 2008-09-11 Routine/Complete Inspection No Violations Noted
1735565 Primary Facility 2008-09-17 Follow-up Inspection Violation(s) Noted After reviewing the completion report, the well has been found to have insufficient surface casing for the observed 435 psi (recorded 9/11/08 - inspection record #1734558). I met with Ray Hepler on location and discussed options to get the well in compliance. He agreed to run approximately 1200 to 1300 feet of 2 3/8 upset tubing that would bring the well into compliance for allowable pressure. NOV to be sent for excessive casing seat pressure.
1738853 Primary Facility 2008-09-30 Compliance Evaluation No Violations Noted Pressure on casing has been brought into compliance. Pressure is 160#.
1940833 Primary Facility 2011-01-04 Routine/Complete Inspection No Violations Noted
1944712 Primary Facility 2011-01-20 Routine/Complete Inspection No Violations Noted
2461461 Primary Facility 2016-03-02 Routine/Complete Inspection No Violations Noted

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1735565 547533 09/17/2008 2008-09-17 78.73B - Excessive casing seat pressure Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
547533 238928 NOV - Notice of Violation Comply/Closed 2008-09-30

For data sources see[7]

References