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37-065-01563

Well Details

Well ID: 37-065-01563
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Country: United States
State: Pennsylvania
County: Jefferson
Municipality: Oliver Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: MAUK 1
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.024960
Longitude: -79.108550

For data sources see[1][2][3]

Well History

Date Event
1952-12-01 Drilling Completion
2001-05-11 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 HANLEY & BIRD INC 367.00 365 0.00 0 0.00 0
1996 HANLEY & BIRD INC 1074 365 0.00 0 0.00 0
1997 HANLEY & BIRD INC 1010 365 0.00 0 0.00 0
1998 HANLEY & BIRD INC 395 365 0.00 0 0.00 0
1999 HANLEY & BIRD INC 1212 365 0.00 0 0.00 0
2000 HANLEY & BIRD INC 1119 365 0.00 0 0.00 0
2001 HANLEY & BIRD INC 465 365 0.00 0 0.00 0
2002 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2003 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2004 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2005 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2006 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2007 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2008 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2009 HANLEY & BIRD INC 1750.00 365 0.00 0 0.00 0
2010 HANLEY & BIRD INC 443.83 365 0.00 0 0.00 0
2011 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2012 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2013 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2014 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2015 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2016 ALLIANCE PETRO CO LLC 0.00 0 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 0.00 0 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2809420 Primary Facility 2018-11-27 Routine/Partial Inspection Violation(s) Noted This well was equipped for production. The valves on this well were currently in a closed position. There was no production reported for this well on the 2017 annual production report. Well is abandoned.

There as a smell of gas at the site.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2809420 834923 2018-11-27 2019-03-07 OGA3220(A) Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
834923 369711 NOV - Notice of Violation 2019-03-07
834923 372946 COA - Consent Order and Agreement

For data sources see[6]

References