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37-065-01213

Well Details

Well ID: 37-065-01213
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Country: United States
State: Pennsylvania
County: Jefferson
Municipality: Winslow Township
Operator Name: SENECA RESOURCES CO LLC
Well Pad ID:
Farm/Lease Name: HARRY H NOLPH
License Status: Plugged and Abandoned
Spud Date: 1938-10-02
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.047969
Longitude: -78.892289

For data sources see[1][2][3]

Well History

Date Event
1938-12-09 Drilling Completion
2001-05-16 Old Well
2018-08-06 Begin Plugging
2018-10-09 Finished Plugging
2019-06-14 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 NATL FUEL GAS SUPPLY CORP 4616.00 365 0.00 0 0.00 0
1992 NATL FUEL GAS SUPPLY CORP 4516.00 366 0.00 0 0.00 0
1993 NATL FUEL GAS SUPPLY CORP 4380.00 365 0.00 0 0.00 0
1994 NATL FUEL GAS SUPPLY CORP 4380.00 365 0.00 0 0.00 0
1995 SENECA RESOURCES CO LLC 1983.20 359 0.00 0 0.00 0
1996 SENECA RESOURCES CO LLC 3878 365 0.00 0 0.00 0
1997 SENECA RESOURCES CO LLC 2547 365 0.00 0 0.00 0
1998 SENECA RESOURCES CO LLC 2889 365 0.00 0 0.00 0
1999 SENECA RESOURCES CO LLC 640 365 0.00 0 0.00 0
2000 SENECA RESOURCES CO LLC 4392 365 0.00 0 0.00 0
2001 SENECA RESOURCES CO LLC 4380 365 0.00 0 0.00 0
2002 SENECA RESOURCES CO LLC 3648 365 0.00 0 0.00 0
2003 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2004 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2006 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2007 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2008 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2009 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2010 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2011 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2012 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2013 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2014 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2015 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2016 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2017 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2018 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2018 SENECA RESOURCES CO LLC Produced Fluid 95.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1768575 Primary Facility 2009-02-11 Complaint Inspection No Violations Noted
2769295 Primary Facility 2018-08-28 Routine/Partial Inspection No Violations Noted At the time of inspection, Alco Well Services was cleaning out the well. They have made it to a depth of 2160'. The record has TD at 2743'. A lined pit is being used at the site.
2771985 Primary Facility 2018-09-06 Routine/Partial Inspection No Violations Noted At the time of inspection, Alco Well Services was not working at this site today. Spoke to company man and was told that the current depth is at 2260'. This is about 200' off of the Tiona. Clean out will resume next week. Only a small amount of waste was in the pit.
2778554 Primary Facility 2018-09-20 Routine/Partial Inspection No Violations Noted At the time of inspection, no activity was taking place. Rig operators were at another plug job. For 6 days in a row, depth has been like a yo-yo, going from between 2290' and 2325'. Well keeps caving back in overnight. They were at 2295' when they shut down. The top of the Tiona is at 2470'. I verbally agreed to an attainable bottom, whatever depth that is when they are back to the rig. Operator will set a 550' cement plug at this depth. Cementing is planned for Tuesday.
2781131 Primary Facility 2018-09-26 Routine/Partial Inspection No Violations Noted At the time of inspection, Alco crew onsite setting up to cement tomorrow. A bond log had been run on the 4" and found it to be tight from 650'-920'. The bottom of the pipe was tight as well. Rig pulled at close to 40,000 lbs and only got a little bit of stretch and ach attempt was getting worse. The 4" was cut at 1270' and still no movement. Plan was to perforate above 1270' with 8 sets of shots to 920'. Then cement to 650', cut the 4" and pull, then shoot the 6" near bottom to squeeze some cement down the backside.
2781574 Primary Facility 2018-09-27 Routine/Partial Inspection No Violations Noted At the time of inspection, Alco crew just finished up with cementing. The 4" casing was perforated at 1250', 1225', 1175', 1125', 1075', 1025', 975', and 930'. Each perf had 4 shots. After this, cement was pumped from 2275' to calculated 1720'. This was later tagged at 1948', so cement was going down the backside of the perfs. Gel was then set to 1250'. Todays cement job was from here to a calculated 720'. I received a phone call later in the day that this was tagged at 787'.
2785453 Primary Facility 2018-10-04 Routine/Partial Inspection No Violations Noted At the time of inspection, no activity was taking place. Alco rig is laid down. Well only needs pea gravel added and a marker. Plan is to return next week to do this when things dry out some.

The 6" casing had been perforated since last inspection. 4 shots per perf were used at 625', 600', 575', and 525'. Cement was then pumped from 787' to a tagged top at 513'.

2788317 Primary Facility 2018-10-11 Routine/Partial Inspection No Violations Noted At the time of inspection, no activity was taking place. Pea gravel has been added to surface. Marker has not been placed yet. Equipment remains onsite. The pit has been back filled.
2801630 Primary Facility 2018-11-13 Administrative/File Review No Violations Noted

For data sources see[7]

References