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| Well ID: 37-065-01104 | Loading map...
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| Country: United States | |
| State: Pennsylvania | |
| County: Jefferson | |
| Municipality: Rose Township | |
| Operator Name: DIVERSIFIED OIL & GAS LLC | |
| Well Pad ID: | |
| Farm/Lease Name: JAMES T BURNS 5567 | |
| License Status: ACTIVE | |
| Spud Date: | |
| Permit Date: | |
| Well Type: GAS | |
| Unconventional Well: N | |
| Configuration: Vertical Well | |
| Conservation: No | |
| Latitude: 41.0970 | |
| Longitude: -79.1016 |
| Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
|---|---|---|---|---|---|---|---|
| 1991 | NATL FUEL GAS SUPPLY CORP | 1908.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 1992 | NATL FUEL GAS SUPPLY CORP | 1913.00 | 366 | 0.00 | 0 | 0.00 | 0 |
| 1993 | NATL FUEL GAS SUPPLY CORP | 1908.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 1994 | NATL FUEL GAS SUPPLY CORP | 1908.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 1995 | SENECA RESOURCES CO LLC | 1983.20 | 359 | 0.00 | 0 | 0.00 | 0 |
| 1996 | SENECA RESOURCES CO LLC | 1272 | 365 | 0.00 | 0 | 0.00 | 0 |
| 1997 | SENECA RESOURCES CO LLC | 1520 | 365 | 0.00 | 0 | 0.00 | 0 |
| 1998 | SENECA RESOURCES CO LLC | 850 | 365 | 0.00 | 0 | 0.00 | 0 |
| 1999 | SENECA RESOURCES CO LLC | 377 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2000 | SENECA RESOURCES CO LLC | 378 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2001 | SENECA RESOURCES CO LLC | 377 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2002 | SENECA RESOURCES CO LLC | 377 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2003 | SENECA RESOURCES CO LLC | 475 | 364 | 0.00 | 0 | 0.00 | 0 |
| 2004 | SENECA RESOURCES CO LLC | 620 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2006 | SENECA RESOURCES CO LLC | 1,198.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2007 | SENECA RESOURCES CO LLC | 188.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2008 | SENECA RESOURCES CO LLC | 1039.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2009 | SENECA RESOURCES CO LLC | 648.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2010 | SENECA RESOURCES CO LLC | 826.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2011 | SENECA RESOURCES CO LLC | 270.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2012 | SENECA RESOURCES CO LLC | 48.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2013 | SENECA RESOURCES CO LLC | 1.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2014 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2015 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2016 | DIVERSIFIED OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2017 | DIVERSIFIED OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2018 | DIVERSIFIED OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[4]
| Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|---|
| 2811999 | Primary Facility | 2018-12-05 | Routine/Partial Inspection | Violation(s) Noted | This well was equipped for production. The valves on this well were currently in a closed position. There was no production reported for this well on the 2017 annual production report. Well is abandoned. |
| 2831957 | Primary Facility | 2019-01-17 | Routine/Partial Inspection | No Violations Noted | Met with welltender at the site to request that the well be blown down. Prior to this happening, there was 0% methane on the 2 annuli. There was also 104.2 psi on the 2" casing. The pipe was parted at a union to blow it down. It was requested that the well be left open. Gas was still blowing out fairly hard when leaving site. |
| 2836483 | Primary Facility | 2019-02-01 | Routine/Partial Inspection | No Violations Noted | At the time of inspection, well was still venting. Some gas was coming out, but not a lot. Well will remain open during the gas migration case. |
| Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
|---|---|---|---|---|---|---|
| 2811999 | 835575 | 2018-12-05 | 2019-03-07 | OGA3220(A) | Environmental Health & Safety |
| Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
|---|---|---|---|---|---|---|---|
| 835575 | 369710 | NOV - Notice of Violation | 2019-03-07 | ||||
| 835575 | 372946 | COA - Consent Order and Agreement |
For data sources see[5]