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37-063-36519

Well Details

Well ID: 37-063-36519
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Black Lick Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: RALPH SHAFFER 5A
License Status: PLUGGED & ABANDONED
Spud Date: 2010-01-11
Permit Date: 2009-04-17
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.482686
Longitude: -79.271692

For data sources see[1][2][3]

Well History

Date Event
2009-04-17 New Permit Application
2010-01-06 Performed Spud Operation
2010-01-11 Drilling Completion
2010-01-19 Drilling Completion
2010-01-25 Perforation
2010-04-21 NEWLY DRILLED
2010-04-21 SKIDDED RIG
2010-10-08 FULLY PLUGGED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 PHILLIPS EXPLORATION INC 5,977.00 256 0.00 0 0.00 0
2011 PHILLIPS EXPLORATION INC 5,709.00 319 0.00 0 0.00 0
2012 XTO ENERGY INC 7,157.00 366 0.00 0 0.00 0
2013 XTO ENERGY INC 8,835.00 365 0.00 0 0.00 0
2014 XTO ENERGY INC 5,638.00 365 0.00 0 0.00 0
2015 XTO ENERGY INC 5,296.00 365 0.00 0 0.00 0
2016 XTO ENERGY INC 4,622.00 366 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 3,145.00 334 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 5,937.00 365 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 6,024.00 365 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1828213 Primary Facility 2009-09-10 Drilling/Alteration No Violations Noted According to records, well permit issued on 4/17/09. Site pad completed. Two pits completed not aligned with plastic. Based on site conditions, no indication of IW issues at the site. Well sign and E&S plan located at entrance way of site pad. No E&S issues at the site. Well marked with survey marker.
1849067 Primary Facility 2009-12-03 Routine/Complete Inspection No Violations Noted At the time of inspection, the well was staked, not yet drilled. The site was properly signed with E&S plan available for review. Site appeared to be constructed following E&S plan. Pit dug,but unlined. Filter fabric fence was installed on the below gradient side of the pad. Noted various areas of E&S concerns which I am recommending be addressed promptly prior to drilling. First, there were notable areas of prior disturbance occurring from around drill pit and running down gradient towards silt fence. This concern can be addressed by installing a rocked lined interceptor ditch. Access road entrance is stable, but noted that access road to well site was muddy. I also observed some disturbance to the field beside the access road, that may needed to be reseeded. Well site was temporarily reseeded and some growth was observed.
1855472 Primary Facility 2010-01-07 Drilling/Alteration No Violations Noted According to records, well permit issued on 4/17/09. Site pad completed. Two pits completed with 20 ml plastic. Based on site conditions, no indication of IW issues at the site. Well sign and E&S plan located at entrance way of site pad. No E&S issues at the site. PC had rig set and was starting to drill the conductor pipe on 1/8/10. TSS filter was present.
1856134 Primary Facility 2010-01-14 Routine/Complete Inspection No Violations Noted Drilling rig located onsite and drilling was ongoing at the time of the inspection. Below grade pit located onsite and had more than two feet of lined freeboard. Observed no accelerated erosion & sedimentation with respect to the acess road. The operator should continue to monitor the erosion controls and the stability of the access road until well development and site restoration activities are completed.
1856359 Primary Facility 2010-01-14 Drilling/Alteration No Violations Noted According to records, well permit issued on 4/17/09. Site pad completed. Two pits completed with 20 ml plastic. Based on site conditions, no indication of IW issues at the site. Well sign and E&S plan located at entrance way of site pad. No E&S issues at the site. PC drilled well on 1/11/10 and hit open mine around 460¿. PC called Rick Hoover (DEP) and determined to abandoned this well and skid the rig. PC filled bore hole with 12 tons of gravel and cemented the remaining hole. PC moved rig 20 ft north of former well. Well set conductor pipe at 13 3/8¿ to 18¿ and second string at 9 5/8¿ to 514¿ with 240 sks class A. Mine shaft hit at 468 ft to 474 ft. Third string 7¿ pipe set at 1241¿ with 150 sks50/50 3% and 75 sks class A. Anticipated depth at 3835¿.
1930551 Primary Facility 2010-11-22 Site Restoration No Violations Noted At the time of inspection, well drilled and in production. Tag present. Rig skid from R Shaffer 5. Site adequately and uniformly restored with successful vegetative growth. No accelerated erosion or sedimentation issues observed. Access road stable. Brine tank sound.
1964037 Primary Facility 2011-04-06 Routine/Complete Inspection No Violations Noted Tag, tank, e&s ok.
1971883 Primary Facility 2011-05-09 Site Restoration No Violations Noted At the time of inspection, well tag present, well drilled and in production. Drilling completed 01/19/2010. Site adequately and uniformly restored with vegetative cover and rock capable of resisting erosion. All temporary bmp¿s appear to be removed. Access road stable. No accelerated erosion/sedimentation or industrial waste issues noted. No violations noted during this inspection.
2321507 Primary Facility 2014-11-13 Routine/Complete Inspection No Violations Noted At time of inspection, well drilled and equipped for production. According to records, drilling occurred 1/11/2010-1/19/2010. Well tag present, legible. Brine tank sound, located on gravel pad. Faint gas odor noted.
2515012 Primary Facility 2016-08-10 Routine/Complete Inspection No Violations Noted 8/10/2016 - Produced fluids tank, annulus closed.

For data sources see[6]

References