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37-063-34128

Well Details

Well ID: 37-063-34128
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Conemaugh Township
Operator Name: US ENERGY EXPLORATION CORP
Well Pad ID:
Farm/Lease Name: CORRIDONI 4
License Status: ACTIVE
Spud Date: 2005-03-21
Permit Date: 2005-01-28
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.536743
Longitude: -79.429891

For data sources see[1][2][3]

Well History

Date Event
2005-01-28 New Permit Application
2005-03-19 Performed Spud Operation
2005-03-23 Drilling Completion
2006-05-04 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2005 US ENERGY EXPLORATION CORP 8572 210 0.00 0 0.00 0
2008 US ENERGY EXPLORATION CORP 3893.00 360 0.00 0 0.00 0
2009 US ENERGY EXPLORATION CORP 2587.00 360 0.00 0 0.00 0
2010 US ENERGY EXPLORATION CORP 2,569.00 360 0.00 0 0.00 0
2011 US ENERGY EXPLORATION CORP 2,072.00 360 0.00 0 0.00 0
2012 US ENERGY EXPLORATION CORP 533.00 360 0.00 0 0.00 0
2013 US ENERGY EXPLORATION CORP 920.00 360 0.00 0 0.00 0
2014 US ENERGY EXPLORATION CORP 1,072.00 365 0.00 0 0.00 0
2015 US ENERGY EXPLORATION CORP 825.00 365 0.00 0 0.00 0
2016 US ENERGY EXPLORATION CORP 881.00 330 0.00 0 0.00 0
2017 US ENERGY EXPLORATION CORP 387.00 134 0.00 0 0.00 0
2018 US ENERGY EXPLORATION CORP 1,027.00 365 0.00 0 0.00 0
2019 US ENERGY EXPLORATION CORP 529.00 270 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1883565 Primary Facility 2010-05-07 Routine/Complete Inspection No Violations Noted Based on record, permit was approved on 1/13//05. Well installed on 3/23/05 to a depth of 4263 ft. Report submitted and approved on 3/23/05. Well completed with 8¿ pipe reduced to 4 ¿pipe reduced to 2¿ production pipe and multiple shut off valves. Production equipment consists of heater, separator, 50 bbl (<10 bbl) and dual phase data logger (150 psi/5 psi). At the time of inspection, no IW issues at the site. However, site shows signs of no restoration. Forwarded pictures and inspection to WQ personnel for further evaluation. E&S issues at the site. No signs of fluid or gas leakage around well head. Well tag was present.

For data sources see[6]

References