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| Well ID: 37-063-32524 | Loading map...
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| Country: United States | |
| State: Pennsylvania | |
| County: Indiana | |
| Municipality: Burrell Township | |
| Operator Name: FATE VENTURES LLC | |
| Well Pad ID: | |
| Farm/Lease Name: ZIAS 1 | |
| License Status: ACTIVE | |
| Spud Date: 2000-06-06 | |
| Permit Date: 2000-03-20 | |
| Well Type: GAS | |
| Unconventional Well: N | |
| Configuration: Vertical Well | |
| Conservation: No | |
| Latitude: 40.467417 | |
| Longitude: -79.239611 |
| Date | Event |
|---|---|
| 2000-03-20 | New Permit Application |
| 2000-06-05 | Performed Spud Operation |
| 2000-06-08 | Drilling Completion |
| 2001-03-07 | NEWLY DRILLED |
| 2002-03-14 | Perforation |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
|---|---|---|---|---|---|---|---|
| 2000 | BELDEN & BLAKE CORP | 3167 | 366 | 0.00 | 0 | 0.00 | 0 |
| 2001 | BELDEN & BLAKE CORP | 6821 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2002 | BELDEN & BLAKE CORP | 5378 | 365 | 0 | 0 | 0.00 | 0 |
| 2003 | BELDEN & BLAKE CORP | 3229 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2004 | BELDEN & BLAKE CORP | 3868 | 366 | 0.00 | 0 | 0.00 | 0 |
| 2005 | BELDEN & BLAKE CORP | 2935 | 365 | 0 | 365 | 0.00 | 0 |
| 2006 | BELDEN & BLAKE CORP | 2,801.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2007 | BELDEN & BLAKE CORP | 3,564.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2008 | BELDEN & BLAKE CORP | 6,636.79 | 366 | 0.00 | 0 | 0.00 | 0 |
| 2009 | BELDEN & BLAKE CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2010 | KEYROCK ENERGY LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2011 | KEYROCK ENERGY LLC | 294.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2012 | KEYROCK ENERGY LLC | 342.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2013 | KEYROCK ENERGY LLC | 12.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2014 | KEYROCK ENERGY LLC | 1.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2015 | KEYROCK ENERGY LLC | 1.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2016 | KEYROCK ENERGY LLC | 1.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2018 | KEYROCK ENERGY LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
| Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
|---|---|---|---|---|---|
| 2002 | BELDEN & BLAKE CORP | Brine | 7,812.00 Bbl | Treated On-Site, NPDES Discharge | |
| 2003 | BELDEN & BLAKE CORP | Brine | 8,184.00 Bbl | Treated On-Site, NPDES Discharge | PA0206075 |
| 2004 | BELDEN & BLAKE CORP | Brine | 6,436.86 Bbl | Treated On-Site, NPDES Discharge | PA0206075 |
| 2005 | BELDEN & BLAKE CORP | Brine | 7,810.00 Bbl | Treated On-Site, NPDES Discharge | PA0206075 |
| 2006 | BELDEN & BLAKE CORP | Brine | 8,451.00 Bbl | Treated On-Site, NPDES Discharge | PA0206075 |
For data sources see[6]
| Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|---|
| 1819509 | Primary Facility | 2009-08-07 | Routine/Complete Inspection | No Violations Noted | Well drilled on 6/8/00 to depth of 1,126 ft. Report submitted and approved to the DEP on 3/29/02. Well designed for Coal Bed Methane collection. Well head consisted of 4 ¿pipe reduced to 2¿ production. Dual data logger showed 30 psi/ 0 psi readings. Pump jack located at the well and was disconnected from the well during the inspection. At the time of inspection, no E&S issues at the site. |
For data sources see[7]