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Well ID: 37-063-25445 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: East Wheatfield Township | |
Operator Name: VERNARD L SHUMAKER | |
Well Pad ID: | |
Farm/Lease Name: JOHN OFMAN 1F261 | |
License Status: | |
Spud Date: 1980-09-05 | |
Permit Date: 1980-04-08 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.482653 | |
Longitude: -79.070267 |
Date | Event |
---|---|
1980-04-08 | New Permit Application |
1980-09-05 | Performed Spud Operation |
1980-09-10 | Drilling Completion |
1980-09-23 | Perforation |
1980-11-03 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | ENERGY PROD CO | 675.00 | 63 | 0.00 | 0 | 0.00 | 0 |
1992 | ENERGY PROD CO | 735.00 | 94 | 0.00 | 0 | 0.00 | 0 |
2010 | VERNARD L SHUMAKER | 776.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | VERNARD L SHUMAKER | 633.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2013 | VERNARD L SHUMAKER | 518.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | VERNARD L SHUMAKER | 611.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | VERNARD L SHUMAKER | 286.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | VERNARD L SHUMAKER | 330.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | VERNARD L SHUMAKER | 321.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | VERNARD L SHUMAKER | 256.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2589621 | Primary Facility | 2017-05-02 | Routine/Complete Inspection | Pending | At time of inspection, well drilled and appears equipped for production. Well label present. Department recommends operator replace well tag on well in a legible, visible, and permanent manner per current regulations. |
2592879 | Primary Facility | 2017-05-03 | Routine/Complete Inspection | In Compliance with Policy | Admin inspection conducted in response to inspection record 2589621. At 0759, operator representative Vern Shumaker contacted the Department via phone.
Per Mr. Shumaker: He is en route to the well site. Booms and absorbent pads will be utilized to control and remediate the release and all impacted materials will be excavated. The tank will be emptied and removed. A quantity released will be provided to the Department. Mr. Shumaker stated that he believed the tank to be empty, so it must be residual oil within the tank that is leaking. Operator appears to be in compliance with policy at this time. Inspection record 2589621 remains pending upon operator response and further investigation. |
2598015 | Primary Facility | 2017-05-15 | Administrative/File Review | In Compliance with Policy | Admin inspection conducted in response to inspection record 2589621.
At 1032, operator representative Vern Shumaker notified the Department via voicemail that a water truck is going to empty the remaining fluids from the tank and then the tank will be removed from the well site. Operator appears to be in compliance with policy at this time. Inspection record 2589621 remains pending upon operator response and further investigation. |
2602583 | Primary Facility | 2017-05-26 | Administrative/File Review | In Compliance with Policy | Admin inspection conducted in response to inspection record 2589621.
At 0719, Department spoke to Operator representative Vern Shumaker via phone. Per Mr. Shumaker: The tank has been emptied and is scheduled to be removed from the location early next week. Mostly rainwater was released because it had been entering through the top of the tank. An estimated release of 20 gallons oil and water occurred. At this time all visibly impacted soils have been excavated in accordance with the Department's Spill Policy. Additional excavation may be necessary upon removal of the tank. According to Mr. Shumaker: The well site is checked twice a month and had not been leaking during the last site visit. The source of the leak was due to a leaking 3/8 fitting on the sight glass. The leak was initially stopped by replacing the fitting with a plug until the tank could be emptied and removed. Mr. Shumaker agreed to provide pictures to the Department. The Department is requesting the Operator submit the waste disposal m |
2604543 | Primary Facility | 2017-06-01 | Administrative/File Review | In Compliance with Policy | Admin inspection conducted in response to inspection record 2589621.
Operator representative Vern Shumaker notified Department that the tank has been extracted from the well site, the contaminated soils excavated, and there is no indication of saturation of oil. Operator appears to be in compliance with policy at this time. Inspection record 2589621 remains pending upon further operator response. |
2604548 | Primary Facility | 2017-06-01 | Administrative/File Review | In Compliance with Policy | Admin inspection conducted in response to inspection record 2589621.
Operator representative Vernard Shumaker provided pictures of area of excavation. Operator appears to be in compliance with policy at this time. Inspection record 2589621 remains pending upon further operator response. |
2605574 | Primary Facility | 2017-06-07 | Administrative/File Review | In Compliance with Policy | Admin inspection conducted in response to inspection record 2589621.
Operator representative Vernard Shumaker provided pictures of area of remediation. Department recommends operator continue to monitor and maintain site as necessary in order to ensure greater than 70% uniform and adequate vegetative growth is achieved. Operator appears to be in compliance with policy at this time. Previously requested waste manifests not yet received by the Department. Inspection record 2589621 remains pending at this time. |
2615680 | Primary Facility | 2017-07-05 | Administrative/File Review | In Compliance with Policy | Admin inspection conducted in response to inspection record 2589621.
At 1418, Department spoke to Operator representative Vernard Shumaker via phone. Mr. Shumaker notified the Department that the contaminated soils are currently awaiting proper disposal. Upon proper disposal, the waste manifests will be provided to the Department. Operator appears to be in compliance with policy at this time.Inspection record 2589621 remains pending at this time. |
For data sources see[6]