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37-063-23205

Well Details

Well ID: 37-063-23205
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: White Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: ALVIE E FISHER 1
License Status: ACTIVE
Spud Date: 1976-02-12
Permit Date: 1975-10-20
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.602371
Longitude: -79.138601

For data sources see[1][2][3]

Well History

Date Event
1975-10-20 New Permit Application
1976-02-12 Performed Spud Operation
1976-04-19 Drilling Completion
1976-04-26 Perforation
1976-05-17 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 5306.00 364 0.00 0 0.00 0
1992 4996.00 365 0.00 0 0.00 0
1993 4812.00 364 0.00 0 0.00 0
1994 4772.00 365 0.00 0 0.00 0
1995 5050.00 309 0.00 0 0.00 0
1996 5050 365 0.00 0 0.00 0
1998 2982 362 0.00 0 0.00 0
1999 CONSOL GAS CO 7016 365 0.00 0 0.00 0
2000 CONSOL GAS CO 4866 365 0.00 0 0.00 0
2001 CONSOL GAS CO 5097 365 0.00 0 0.00 0
2002 CONSOL GAS CO 4908 365 0.00 0 0.00 0
2003 CONSOL GAS CO 5,001.00 365 0.00 0 0.00 0
2005 CONSOL GAS CO 3829 365 0.00 0 0.00 0
2006 CONSOL GAS CO 2,809.00 365 0.00 0 0.00 0
2007 CONSOL GAS CO 2416.00 365 0.00 0 0.00 0
2008 CONSOL GAS CO 3058.00 365 0.00 0 0.00 0
2009 CONSOL GAS CO 2116.00 365 0.00 0 0.00 0
2010 CONSOL GAS CO 1,702.00 365 0.00 0 0.00 0
2011 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2012 CNX GAS CO LLC 2,886.00 366 0.00 0 0.00 0
2013 CNX GAS CO LLC 3,112.00 365 0.00 0 0.00 0
2014 CNX GAS CO LLC 2,576.00 365 0.00 0 0.00 0
2015 CNX GAS CO LLC 894.00 365 0.00 0 0.00 0
2016 CNX GAS CO LLC 1,562.00 366 0.00 0 0.00 0
2017 CNX GAS CO LLC 1,630.00 334 0.00 0 0.00 0
2018 CNX GAS CO LLC 1,457.00 306 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 2,958.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2005 CONSOL GAS CO Brine 30.00 Bbl Brine or Industrial Waste Treatment Plt PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2665226 Primary Facility 2017-11-29 Routine/Complete Inspection No Violations Noted
2665419 Primary Facility 2017-11-29 Incident- Response to Accident or Event No Violations Noted At time of inspection well appears equipped for production. CNX rep Scott Bowers present during inspection.

Inspection conducted in response to a meter fire on 11-27-17. The meter associated with this well caught fire on 11-27-17 with emergency personnel (Indiana Fire Association) on site around 18:00. The meter is approximately 1400 feet from this well. According to Mr. Bowers the meter is only associated with this well and connects to a transmission line operated by Peoples Natural Gas. Mr. Bowers was at the meter site to remove equipment damaged during the fire.

For data sources see[7]

References