If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
| Well ID: 37-063-22502 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.647468,"lon":-79.139871,"icon":""}]} |
| Country: United States | |
| State: Pennsylvania | |
| County: Indiana | |
| Municipality: White Township | |
| Operator Name: CHESTNUT RIDGE ENERGY OF PA LLC | |
| Well Pad ID: | |
| Farm/Lease Name: IRA J MARTIN 1 | |
| License Status: ACTIVE | |
| Spud Date: 1974-03-26 | |
| Permit Date: 1974-03-19 | |
| Well Type: GAS | |
| Unconventional Well: N | |
| Configuration: Vertical Well | |
| Conservation: No | |
| Latitude: 40.647468 | |
| Longitude: -79.139871 |
| Date | Event |
|---|---|
| 1974-03-19 | New Permit Application |
| 1974-03-26 | Performed Spud Operation |
| 1974-04-01 | Drilling Completion |
| 1974-05-01 | Perforation |
| 1975-05-16 | NEWLY DRILLED |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
|---|---|---|---|---|---|---|---|
| 2010 | EAST RESOURCES MGMT LLC | 4,002.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2011 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2012 | CHESTNUT RIDGE ENERGY OF PA LLC | 20.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2013 | CHESTNUT RIDGE ENERGY OF PA LLC | 0.01 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2014 | CHESTNUT RIDGE ENERGY OF PA LLC | 0.01 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2015 | CHESTNUT RIDGE ENERGY OF PA LLC | 0.01 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
| Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
|---|---|---|---|---|---|
| 2010 | EAST RESOURCES MGMT LLC | Produced Fluid | 86.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
For data sources see[6]
| Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|---|
| 2401163 | Primary Facility | 2015-06-24 | Complaint Inspection | No Violations Noted | Gas well was in production. Gas leak occurring at the well head at the bung on the coupling piping. Called Chestnut Ridge Energy of Pa to repair leak. |
| 2483980 | Primary Facility | 2016-05-09 | Complaint Inspection | Violation(s) Noted | Well tag present at the well head. Natural gas was venting from a crack in the metal surface casing. Crack was approximately ½” in length underneath the reducer fitting. At the wellhead, DEP used a 62S meter and obtained 100 % gas reading at the crack in metal. DEP took readings surrounding the well head at approximately 10 feet away and gas readings were less than 10 % gas reading. Upon a file review, Chestnut Ridge Energy has not submitted production reports nor Mechanical Integrity reports to the DEP since 2012. Chestnut Ridge was notified of the instinct and plans on bringing a surface rig to site to repair leak. |
| Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
|---|---|---|---|---|---|---|
| 2483980 | 759238 | 2016-05-09 | 2016-05-11 | 78.12 | Administrative | |
| 2483980 | 759239 | 2016-05-09 | 2016-05-11 | 78.89(a) | Environmental Health & Safety | |
| 2483980 | 759240 | 2016-05-09 | 2016-05-11 | 78.88(a) | Administrative |
| Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
|---|---|---|---|---|---|---|---|
| 759238 | 342896 | NOV - Notice of Violation | 2016-05-16 | ||||
| 759238 | 344738 | ADORD - Administrative Order | 2016-07-05 | ||||
| 759239 | 342896 | NOV - Notice of Violation | 2016-05-16 | ||||
| 759239 | 344738 | ADORD - Administrative Order | 2016-07-05 | ||||
| 759240 | 342896 | NOV - Notice of Violation | 2016-05-16 | ||||
| 759240 | 344738 | ADORD - Administrative Order | 2016-07-05 |
For data sources see[7]