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Well ID: 37-059-26897 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Greene | |
Municipality: Dunkard Township | |
Operator Name: CHEVRON APPALACHIA LLC | |
Well Pad ID: 152180 | |
Farm/Lease Name: HENDRICKSON 4H | |
License Status: | |
Spud Date: | |
Permit Date: 2015-06-22 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 39.771689 | |
Longitude: -80.027136 |
Date | Event |
---|---|
2015-06-22 | New Permit Application |
2015-09-02 | Performed Spud Operation |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2015 | CHEVRON APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | CHEVRON APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | CHEVRON APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2019 | CHEVRON APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2015 | CHEVRON APPALACHIA LLC | Produced Fluid | 50.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123SW001 |
2015 | CHEVRON APPALACHIA LLC | Drilling Fluid Waste | 1,145.83 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123SW001 |
2015 | CHEVRON APPALACHIA LLC | Drill Cuttings | 60.67 Tons | LANDFILL | 100592 |
2015 | CHEVRON APPALACHIA LLC | Drill Cuttings | 233.21 Tons | LANDFILL | 100172 |
2019 | CHEVRON APPALACHIA LLC | Waste Water Treatment Sludge | 9.47 Tons | RESIDUAL WASTE PROCESSING FACILITY | 2014-541 |
2019 | CHEVRON APPALACHIA LLC | Synthetic Liner Materials | 11.18 Tons | LANDFILL | 100172 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2393673 | Primary Facility | 2015-07-01 | Drilling/Alteration | No Violations Noted | HORIZONTAL MARCELLUS, Set conductor @ 53' ( KB ) 6/30/2015. |
2402539 | Primary Facility | 2015-08-04 | Drilling/Alteration | No Violations Noted | HORIZONTAL MARCELLUS, Drilled to 408' ( TD ). Setting Watr Protection Casing to 387' and cementing tonight (8/2/2015).Received call from Chevron explaining Lost Circulation on cement job and plans how to correct the issues. |
2402551 | Primary Facility | 2015-08-06 | Drilling/Alteration | No Violations Noted | HORIZONTAL MARCELLUS, Here is a response from the operator, Rick,as per our discussion on the evening of August 5th, 2015 we perforated from 218' to 220', attempted to establish an injection rate of 5 bpm. We were only able to achieve 2.5 bpm. We then subsequently perforated from 216' to 218'. On the morning of August 6th, 2015 we attempted to establish an injection rate of 5 bpm, and were able to do so with 40 bbls of fresh water. After 40 bbls of water were away we were only able to sustain an injection rate of 2.5 bpm. |
2402578 | Primary Facility | 2015-08-07 | Drilling/Alteration | No Violations Noted | HORIZONTAL MARCELLUS, Arrived on location to discover the 2nd cement job was not successful .They are planning to run ( CBL ) log to determine top of cement. |
2402634 | Primary Facility | 2015-08-21 | Drilling/Alteration | No Violations Noted | HORIZONTAL MARCELLUS, Rig moving back on to # 4 well on (8/16/2015).We did not observe cement to service on our last cement job attempt on the Hendrickson 4H. We will woc 8hrs, we will then drill out to our cement to the FC @364' in order to Re-run a CBL log, if top of cement is below the basket we will perforate @268.The bond log shows little cement behind pipe. The operator decided to set cement plug in 20"casing and move to #3 well. The future plan is to P/A # 4 well pryor to drilling new # 4 well. |
2420193 | Primary Facility | 2015-10-28 | Drilling/Alteration | No Violations Noted | HORIZONTAL MARCELLUS, The operator decided to Plug this well bore to surface .The origional plan is to set a new conductor and re-drill at later date. The new conductor spud is on hold . |
2479127 | Primary Facility | 2016-04-27 | Routine/Complete Inspection | No Violations Noted |
On 04/27/16 at approximately 0830 hours I conducted a routine complete inspection of the site. The Act 9 sign was in place and all required documents were present in the mail box. The site overall was well vegetated. One location to the right side of the access road at the pad is recommended to receive additional seeding and mulch (see photos). There were no violations noted at the time of inspection. |
For data sources see[7]