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37-059-01570

Well Details

Well ID: 37-059-01570
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Country: United States
State: Pennsylvania
County: Greene
Municipality: Richhill Township
Operator Name: LEATHERWOOD INC
Well Pad ID:
Farm/Lease Name: F. P. HEADLEY 1
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: OIL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 39.889181
Longitude: -80.415994

For data sources see[1][2][3]

Well History

Date Event
1902-11-13 Drilling Completion
1903-01-01 Old Well
2015-10-21 Begin Plugging
2015-11-16 Finished Plugging

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 GREENRIDGE OIL CO INC 0.00 0 204.00 365 0.00 0
1997 MTN ENERGY 0.00 0 204 365 0.00 0
1998 MTN ENERGY 0.00 0 188 365 0.00 0
1999 MTN ENERGY 0.00 0 224 365 0.00 0
2001 MTN ENERGY 0.00 0 156 365 0.00 0
2002 MTN ENERGY 0.00 0 148 365 0.00 0
2003 MTN ENERGY 0.00 0 167 365 0.00 0
2004 MTN ENERGY 0.00 0 155 365 0.00 0
2005 LEATHERWOOD INC 0.00 0 85 214 0.00 0
2006 LEATHERWOOD INC 0.00 0 350.00 365 0.00 0
2007 LEATHERWOOD INC 0.00 0 0.00 0 0.00 0
2008 LEATHERWOOD INC 265.00 156 0.00 0 0.00 0
2009 LEATHERWOOD INC 0.00 0 257.00 156 0.00 0
2010 LEATHERWOOD INC 0.00 0 231.00 156 0.00 0
2011 LEATHERWOOD INC 0.00 0 172.00 156 0.00 0
2012 LEATHERWOOD INC 0.00 0 133.00 156 0.00 0
2013 LEATHERWOOD INC 0.00 0 0.00 0 0.00 0
2014 LEATHERWOOD INC 0.00 0 0.00 0 0.00 0
2015 LEATHERWOOD INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2432710 Primary Facility 2015-11-05 Plugging(Includes Plugged/Mined Through) No Violations Noted Coastal Rig #214. Pulled 2,990’ of sucker rods. Pulled 3,012’ of tubing. Pulled 2,354’ of 5 ½” casing. Cement plug set from 3,015’ to 2,000’. Currently pulling 7” casing. Conduct site inspection. Notify operator of erosion and sedimentation control plan deficiencies.
2465337 Primary Facility 2016-02-11 Routine/Complete Inspection Violation(s) Noted On 2/11/2016, I performed an inspection of the CNX FP Headley #1 well plugging site with Joel Keller (DEP/OGI) and Joe Laslo (DEP/SMCI). Present at time of inspection was Doug Dinger (Consol). The site is located in Richhill Twp., Greene County. The inspection was performed as a site inspection after a reported sheen in an unnamed trib. to Pollen Run.

Consol Bailey Mine personnel informed the DEP that an oil sheen was documented in an unnamed trib. to Polen Run during stream monitoring associated with mining of the Bailey 2L longwall panel. At time of inspection a noted weathered brown hydrocarbon material was observed in the unnamed trib. to Polen Run down gradient from the recently plugged FP Headley #1 well site (plugged 11/16/15).

2466352 Primary Facility 2016-03-01 Follow-up Inspection Outstanding Violations - No Viols Req'd On 3/1/2016, I performed an inspection of the CNX FP Headley #1 well plugging site with Joel Keller (DEP/OGI). The site is located in Richhill Twp., Greene County. The inspection was performed as a follow up inspection after a reported sheen in an unnamed trib. to Pollen Run.

Consol Bailey Mine personnel informed the DEP that an oil sheen was documented in an unnamed trib. to Polen Run during stream monitoring associated with mining of the Bailey 2L longwall panel. At time of inspection a noted weathered brown hydrocarbon material was observed in the unnamed trib. to Polen Run down gradient from the recently plugged FP Headley #1 well site (plugged 11/16/15). The booms placed by Consol in the stream channel remain. The seep of hydrocarbon from beneath a rock ledge near the headwaters of the unnamed trib. to Polen Run persists.

2498190 Primary Facility 2016-06-14 Compliance Evaluation No Violations Noted On 6/14/2016, I performed an inspection of the CNX FP Headley #1 well plugging site. The site is located in Richhill Twp., Greene County. The inspection was performed as a compliance evaluation inspection after a reported sheen in an unnamed trib. to Pollen Run.

Consol Bailey Mine personnel informed the DEP that an oil sheen was documented in an unnamed trib. to Polen Run during stream monitoring associated with mining of the Bailey 2L longwall panel. At time of inspection a noted weathered brown hydrocarbon material was observed in the unnamed trib. to Polen Run down gradient from the recently plugged FP Headley #1 well site (plugged 11/16/15). The booms placed by Consol in the stream channel have been removed. The seep of hydrocarbon from beneath a rock ledge near the headwaters of the unnamed trib. to Polen Run has stopped, due to the flow from the seep has stopped. No sheen was noted in the stream channel at time of inspection. Flow in the stream channel has decreased with the mining of the 2L lon

536648 Primary Facility 1988-04-26 Routine/Complete Inspection No Violations Noted E&S OK

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2465337 754467 2016-02-11 2016-07-22 78.54 Environmental Health & Safety
2465337 754469 2016-02-11 2016-07-22 CSL 401 Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
754467 340842 NOV - Notice of Violation 2016-09-09
754469 340842 NOV - Notice of Violation 2016-09-09

For data sources see[6]

References