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37-049-22687

Well Details

Well ID: 37-049-22687
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Country: United States
State: Pennsylvania
County: Erie
Municipality: Waterford Township
Operator Name: MEDINA RES DEV CO LLC
Well Pad ID:
Farm/Lease Name: LEO T & DORIS OLIVER 1
License Status: ABANDONED
Spud Date:
Permit Date: 1983-02-23
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 41.970501
Longitude: -79.991738

For data sources see[1][2][3]

Well History

Date Event
1983-01-01 NEWLY DRILLED
1983-02-23 New Permit Application
1983-08-13 Drilling Completion

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1983 ENERGY CORP OF AMER 888.00 0 0.00 0 0.00 0
1984 ENERGY CORP OF AMER 4,771.00 0 0.00 0 0.00 0
1985 ENERGY CORP OF AMER 5,075.00 0 0.00 0 0.00 0
1991 ENERGY CORP OF AMER 475.00 312 0.00 0 0.00 0
1994 ENERGY CORP OF AMER 1121.00 365 0.00 0 0.00 0
1995 ENERGY CORP OF AMER 703.00 365 0.00 0 0.00 0
1996 ENERGY CORP OF AMER 0.00 0 0.00 0 0.00 0
1997 ENERGY CORP OF AMER 279 214 0.00 0 0.00 0
1998 ENERGY CORP OF AMER 498 306 0.00 0 0.00 0
1999 ENERGY CORP OF AMER 321 335 0.00 0 0.00 0
2000 ENERGY CORP OF AMER 17 31 0.00 0 0.00 0
2001 ENERGY CORP OF AMER 0.00 0 0.00 0 0.00 0
2002 ENERGY CORP OF AMER 284 106 0.00 0 0.00 0
2003 ENERGY CORP OF AMER 190 81 0.00 0 0.00 0
2004 ENERGY CORP OF AMER 99 184 0.00 0 0.00 0
2005 ENERGY CORP OF AMER 149 92 0.00 0 0.00 0
2006 ENERGY CORP OF AMER 119.00 75 0.00 0 0.00 0
2007 ENERGY CORP OF AMER 96.00 65 0.00 0 0.00 0
2008 ENERGY CORP OF AMER 101.00 62 0.00 0 0.00 0
2009 ENERGY CORP OF AMER 183.00 92 0.00 0 0.00 0
2010 ENERGY CORP OF AMER 182.00 334 0.00 0 0.00 0
2012 MEDINA RES DEV CO LLC 0.00 0 0.00 0 0.00 0
2014 MEDINA RES DEV CO LLC 0.00 0 0.00 0 0.00 0
2015 MEDINA RES DEV CO LLC 0.00 0 0.00 0 0.00 0
2016 MEDINA RES DEV CO LLC 0.00 0 0.00 0 0.00 0
2017 MEDINA RES DEV CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
1991 ENERGY CORP OF AMER Brine 27.00 Bbl

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1224877 Primary Facility 2003-04-08 Routine/Complete Inspection Violation(s) Noted
1225821 Primary Facility 2003-04-10 Compliance Evaluation Outstanding Violations - No Viols Req'd Unvented annulus violation repaired. Abandoned NOV just went out.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1224877 345835 04/08/2003 2003-04-08 78.73B - Excessive casing seat pressure Administrative Called Welltender "Roy" in Waterford. He called back by noon that he had dug it up and vented. Checked on the 10th of April and it was done.
1224877 345853 04/08/2003 2003-04-08 210UNPLUG - Failure to plug a well upon abandonment Administrative NOV sent to Indiana address 4/10/03

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
345835 117246 NOV - Notice of Violation Comply/Closed 2003-04-17
345853 117246 NOV - Notice of Violation Comply/Closed 2003-04-17

For data sources see[7]

References