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37-047-01787

Well Details

Well ID: 37-047-01787
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Country: United States
State: Pennsylvania
County: Elk
Municipality: Ridgway Township
Operator Name: ALLEGHENY ENTERPRISES INC
Well Pad ID:
Farm/Lease Name: DALHENBACH
License Status: ABANDONED
Spud Date:
Permit Date:
Well Type: COMB. OIL&GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.447619
Longitude: -78.777888

For data sources see[1][2][3]

Well History

Date Event
1901-01-01 Drilling Completion
2001-08-03 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 ALLEGHENY ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2014 ALLEGHENY ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2015 ALLEGHENY ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2016 ALLEGHENY ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2017 ALLEGHENY ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2018 ALLEGHENY ENTERPRISES INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2391732 Primary Facility 2015-07-14 Routine/Complete Inspection Violation(s) Noted
2463007 Primary Facility 2016-03-09 Routine/Complete Inspection Outstanding Violations - No Viols Req'd
2517547 Primary Facility 2016-09-07 Follow-up Inspection Outstanding Violations - No Viols Req'd
2705513 Primary Facility 2018-03-14 Routine/Complete Inspection Violation(s) & Outstanding Violations This well is abandoned and was originally put in violation on 7/14/2015. Nothing has been done to the well, it is still venting gas and today i can hear fluid bubbling in the tubing which is vented to the atmosphere. There is a potential for a fluid discharge onto the ground from the venting tubing.

I received an email through Rich Nevill (DEP) from Cori Fasy on September 7th 2017 ,stating "The well will either be plugged or we do have some interest from another producer to take the well. They would like to see if they can be put back into production. We should know within 60 days".

2739608 Primary Facility 2018-06-11 Compliance Evaluation Outstanding Violations - Viols Req'd This well is still abandoned. Nothing has been done with this well. It continues to vent gas and you can hear the fluid in the tubing bubbling very close to surface.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2391732 730290 07/14/2015 2015-07-14 OGA 3220(A) - Failure to plug the well upon abandoning it. Environmental Health & Safety
2391732 730299 07/14/2015 2015-07-14 OGA 3220(A) - Failure to plug the well upon abandoning it. Environmental Health & Safety
2705513 810939 2018-03-14 OGA3220(A) Environmental Health & Safety
2705513 810940 2018-03-14 OGA3211(G) Administrative
2705513 810941 2018-03-14 OGA3211(H) Administrative
2739608 819434 2018-06-11 OGA3220(A) Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
730290 356238 NOV - Notice of Violation Superseded 2020-01-13
730290 375774 COA - Consent Order and Agreement $6,500.00 $7,400.00
730299 356238 NOV - Notice of Violation Superseded 2020-01-13
730299 375774 COA - Consent Order and Agreement $6,500.00 $7,400.00
810939 356238 NOV - Notice of Violation
810939 374443 ADORD - Administrative Order Superseded 2019-06-06
810939 375774 COA - Consent Order and Agreement $6,500.00 $7,400.00
810940 356238 NOV - Notice of Violation
810940 374443 ADORD - Administrative Order Superseded 2019-06-06
810940 375774 COA - Consent Order and Agreement $6,500.00 $7,400.00
810941 356238 NOV - Notice of Violation
810941 374443 ADORD - Administrative Order Superseded 2019-06-06
810941 375774 COA - Consent Order and Agreement $6,500.00 $7,400.00

For data sources see[6]

References