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37-047-00463

Well Details

Well ID: 37-047-00463
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Country: United States
State: Pennsylvania
County: Elk
Municipality: Jones Township
Operator Name: SENECA RESOURCES CO LLC
Well Pad ID:
Farm/Lease Name: WILIAM M POTTS
License Status: Plugged and Abandoned
Spud Date: 1934-07-14
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.561568
Longitude: -78.753320

For data sources see[1][2][3]

Well History

Date Event
1934-09-04 Drilling Completion
2019-03-04 Begin Plugging
2019-04-03 Finished Plugging
2019-04-05 Reworked
2019-08-19 Fully Plugged

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 NATL FUEL GAS SUPPLY CORP 3636.00 364 0.00 0 0.00 0
1992 NATL FUEL GAS SUPPLY CORP 3014.00 366 0.00 0 0.00 0
1993 NATL FUEL GAS SUPPLY CORP 3211.00 365 0.00 0 0.00 0
1994 NATL FUEL GAS SUPPLY CORP 4591.00 365 0.00 0 0.00 0
1995 SENECA RESOURCES CO LLC 2336.65 360 0.00 0 0.00 0
1996 SENECA RESOURCES CO LLC 4710 365 0.00 0 0.00 0
1997 SENECA RESOURCES CO LLC 2125 365 0.00 0 0.00 0
1998 SENECA RESOURCES CO LLC 3192 365 0.00 0 0.00 0
1999 SENECA RESOURCES CO LLC 1580 365 0.00 0 0.00 0
2000 SENECA RESOURCES CO LLC 1727 365 0.00 0 0.00 0
2001 SENECA RESOURCES CO LLC 1722 365 0.00 0 0.00 0
2002 SENECA RESOURCES CO LLC 1882 365 0.00 0 0.00 0
2003 SENECA RESOURCES CO LLC 3588 361 0.00 0 0.00 0
2004 SENECA RESOURCES CO LLC 3792 361 0.00 0 0.00 0
2006 SENECA RESOURCES CO LLC 3745.00 365 0.00 0 0.00 0
2007 SENECA RESOURCES CO LLC 3746.00 365 0.00 0 0.00 0
2008 SENECA RESOURCES CO LLC 3541.00 365 0.00 0 0.00 0
2009 SENECA RESOURCES CO LLC 1996.00 365 0.00 0 0.00 0
2010 SENECA RESOURCES CO LLC 625.00 365 0.00 0 0.00 0
2011 SENECA RESOURCES CO LLC 79.00 365 0.00 0 0.00 0
2012 SENECA RESOURCES CO LLC 14.00 365 0.00 0 0.00 0
2013 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2014 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2015 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2016 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2017 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2018 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2019 SENECA RESOURCES CO LLC Produced Fluid 200.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1066834 Primary Facility 2001-10-09 Routine/Complete Inspection No Violations Noted
2665902 Primary Facility 2017-11-30 Routine/Complete Inspection No Violations Noted This well is shut in and not producing at this time. No production has been reported since 2012 and the well is on the consent order agreement with Seneca to be plugged at a later date.
2853101 Primary Facility 2019-03-13 Plugging(Includes Plugged/Mined Through) No Violations Noted This well keeps drinking the cement and LCM they pump down the well. They are going to set a bridge at the bottom of the 3" pipe that is just above the shot hole and then perf the pipe and cement over the formations. After running a log they will shoot the 3" off and pull what they can and cement the remaining hole per regulations. They have a lined pit for cuttings and fluids. The location is frozen.
359302 Primary Facility 1989-03-27 Routine/Complete Inspection No Violations Noted WOLF RUN
384073 Primary Facility 1997-12-04 Routine/Complete Inspection No Violations Noted

For data sources see[8]

References