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37-039-24623

Well Details

Well ID: 37-039-24623
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Country: United States
State: Pennsylvania
County: Crawford
Municipality: Spring Township
Operator Name: KASTLE RESOURCES ENTERPRISES INC
Well Pad ID:
Farm/Lease Name: SLADICK UNIT 1
License Status: PLUGGED & ABANDONED
Spud Date:
Permit Date: 2005-10-07
Well Type: COMB. OIL&GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 41.818844
Longitude: -80.397429

For data sources see[1][2][3]

Well History

Date Event
2005-10-07 New Permit Application
2005-10-23 Performed Spud Operation
2005-11-03 Drilling Completion
2005-11-03 Perforation
2006-03-08 New Permit Application
2007-01-22 NEWLY DRILLED
2007-05-01 Drilling Completion
2007-07-16 FULLY PLUGGED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2005 KASTLE RESOURCES ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2006 KASTLE RESOURCES ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2010 KASTLE RESOURCES ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2011 KASTLE RESOURCES ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2012 KASTLE RESOURCES ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2013 KASTLE RESOURCES ENTERPRISES INC 0.00 0 0.00 0 0.00 0
2014 KASTLE RESOURCES ENTERPRISES INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2006 KASTLE RESOURCES ENTERPRISES INC Brine 30.00 Bbl Reuse other than road spreading

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1494029 Primary Facility 2005-11-09 Routine/Complete Inspection No Violations Noted
1500042 Primary Facility 2005-12-05 Plugging(Includes Plugged/Mined Through) Violation(s) Noted
1502810 Primary Facility 2005-12-12 Plugging(Includes Plugged/Mined Through) Outstanding Violations - No Viols Req'd

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1500042 479031 12/05/2005 2005-12-05 78.85 - Inadequate, insufficient, and/or improperly installed cement Environmental Health & Safety Well was partially plugged from drill rig, Capstar. I found gas boiling from fluid over the top of the well, 78.81(a)(2). I could not see were the gas was leaking from. The operator had the area drained with a backhoe or excavator and determined the

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
479031 203248 NOV - Notice of Violation Comply/Closed 2006-01-18

For data sources see[7]

References