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Well ID: 37-033-26494 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Clearfield | |
Municipality: Bloom Township | |
Operator Name: DEVONIAN RESOURCES INC | |
Well Pad ID: | |
Farm/Lease Name: WALLS 3 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 2007-07-11 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.000089 | |
Longitude: -78.653689 |
Date | Event |
---|---|
2007-07-11 | New Permit Application |
2007-08-31 | Performed Spud Operation |
2007-09-11 | Drilling Completion |
2007-09-19 | Perforation |
2008-01-15 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2008 | DEVONIAN RESOURCES INC | 2412.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | DEVONIAN RESOURCES INC | 3221.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | DEVONIAN RESOURCES INC | 1,823.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | DEVONIAN RESOURCES INC | 782.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | DEVONIAN RESOURCES INC | 1,191.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2013 | DEVONIAN RESOURCES INC | 1,354.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | DEVONIAN RESOURCES INC | 491.00 | 330 | 0.00 | 0 | 0.00 | 0 |
2015 | DEVONIAN RESOURCES INC | 530.00 | 210 | 0.00 | 0 | 0.00 | 0 |
2016 | DEVONIAN RESOURCES INC | 241.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | DEVONIAN RESOURCES INC | 67.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | DEVONIAN RESOURCES INC | 25.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | DEVONIAN RESOURCES INC | 278.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2008 | DEVONIAN RESOURCES INC | Brine | 744.00 Bbl | Municipal Sewage Treatment Plant | |
2009 | DEVONIAN RESOURCES INC | Brine | 255.00 Bbl | Municipal Sewage Treatment Plant | PA0028207 |
2010 | DEVONIAN RESOURCES INC | Produced Fluid | 270.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0028207 |
2011 | DEVONIAN RESOURCES INC | Produced Fluid | 142.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0028207 |
2012 | DEVONIAN RESOURCES INC | Produced Fluid | 120.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0028207 |
2013 | DEVONIAN RESOURCES INC | Produced Fluid | 155.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0028207 |
2014 | DEVONIAN RESOURCES INC | Produced Fluid | 200.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0028207 |
2015 | DEVONIAN RESOURCES INC | Produced Fluid | 130.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0028207 |
2016 | DEVONIAN RESOURCES INC | Produced Fluid | 71.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0101508 |
2016 | DEVONIAN RESOURCES INC | Produced Fluid | 71 Bbl | CENT WASTE TRT FAC NPDES | PA0101508 |
2018 | DEVONIAN RESOURCES INC | Produced Fluid | 40.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0101508 |
2019 | DEVONIAN RESOURCES INC | Produced Fluid | 80.00 Bbl | REUSE AT A CONVENTIONAL WELL SITE IN PA |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1659066 | Primary Facility | 2007-09-11 | Drilling/Alteration | No Violations Noted | MOVING RIG OFF SITE. DRILL PIT HAD ADEQUATE FREEBOARD; NO E&S PROBLEMS ON SITE. |
1682957 | Primary Facility | 2007-12-11 | Drilling/Alteration | No Violations Noted | IN LINE, PRODUCING |
1837545 | Primary Facility | 2009-10-14 | Site Restoration | No Violations Noted | -Well complete and in production. Site recontoured and pit encclosed. |
2749379 | Primary Facility | 2018-07-06 | Incident- Response to Accident or Event | Violation(s) Noted | Department representative Sue Herzing conducted an incident related inspection on July 6, 2018 at Devonian Resources conventional well 033-26494 (Walls 3 Well). A small spill of 15 gallons of brine water was reported to the Department on July 2, 2018 by Joe Thompson of Devonian Resources.
During the inspection I observed a small hole located near the top portion of the poly brine and orange staining down the side of the tank. Wet soil was present during my inspection. I used a soil probe to test for conductivity throughout the wet areas and dry areas. I estimated that the impacted area near the brine tank is 12 ft. wide and bottle necks down to 1.5 ft. wide as it travels down gradient for approximately 60 ft. The wet saturated areas maxed out the soil probe at 4.0 mS/cm. Some standing water was observed and maxed out the water screening conductivity meter at 20.0 mS/cm. In addition, stressed vegetation consisting of evergreen trees and grasses was observed within the brine release pathway. No remediation |
2768535 | Primary Facility | 2018-08-28 | Follow-up Inspection | Outstanding Violations - Viols Req'd | Department representatives Sue Herzing and Sasha Minium conducted a follow up inspection on August 28, 2018 at Devonian Resources conventional well 033-26494 (Walls 3) with Joe Thompson of Devonian Resources. A small spill of 15 gallons of brine water was reported to the Department on July 2, 2018.
To date, the operator has only removed some of the impacted soils. Excavated impact soils remain onsite, wrapped in plastic. The bullet hole within the brine tank has been repaired. Impacted soils still remain present exceeding soil conductivity readings of 1,000 uS/cm. During the site inspection, discussions were had on remediating the site. The operator will be addressing remediation by further excavating impacted soils delineated by the Department during the site inspection. Once excavation is completed, please notify the Department. Impacted soils shall be properly disposed. The previous cited violations on July 6, 2018 remain outstanding. No new violations were cited during this inspection. The outstanding |
2784683 | Primary Facility | 2018-10-04 | Follow-up Inspection | Outstanding Violations - Viols Req'd | Department representatives Sue Herzing conducted a follow up inspection on October 4, 2018 at Devonian Resources conventional well 033-26494 (Walls 3). A small spill of 15 gallons of brine fluids was reported to the Department on July 2, 2018 by the owner/operator Joe Thompson.
To date, the operator has only removed some of the impacted soils. Excavated impacted soils remain onsite and wrapped in plastic. The bullet hole within the brine tank has been repaired. Impacted soils still remain present exceeding soil conductivity readings of 1,000 uS/cm. After leaving the site I called Mr. Thompson and discussed when remedial activities will take place. Mr. Thompson stated that his equipment was tied up with another project currently and anticipates getting to this site within 3 weeks to start remedial work. The operator will be addressing remediation by further excavating impacted soils in accordance with the small spill policy 800-50000-001. Once excavation is completed, please notify the Department. Impact |
2822756 | Primary Facility | 2019-01-04 | Follow-up Inspection | No Violations Noted | Department representatives Sue Herzing conducted a follow up inspection on January 4, 2019 at Devonian Resources Inc. conventional well 033-26494 (Walls 3). A small spill of 15 gallons of brine fluids was reported to the Department on July 2, 2018 by the owner/operator Joe Thompson.
Excavated impacted soils remain onsite and wrapped in plastic. The bullet hole within the brine tank has been repaired. The Department recommends removing the impacted soils wrapped in plastic from the site and properly disposing of them. The Department is requesting a copy of the disposal receipts. The previous cited violations on July 6, 2018 remain outstanding. No new violations were cited during this inspection. The outstanding violations will be closed upon receiving confirmation from the operator that the remedial activities have been completed and upon receiving disposal receipts. |
2856846 | Primary Facility | 2019-03-21 | Follow-up Inspection | Outstanding Violations - Viols Req'd | Department representatives Sue Herzing conducted a follow up inspection on March 21, 2019 at Devonian Resources Inc. conventional well 033-26494 (Walls 3). While onsite I meant will landowner Eric Perks. Mr. Perks stated that this well feeds to their nearby hunting camp located several hundred yards uphill from this location.
A small spill of 15 gallons of brine fluids was reported to the Department on July 2, 2018 by the owner/operator Joe Thompson. Excavated impacted soils remain onsite and wrapped in plastic. Serval holes and/or tears were observed in the plastic. A field soil probe reading was taken where a tear in the plastic occurred; reading > 4.00 mS/cm. Since this small spilled occurred over 8+ months ago the Department has been recommending removing the impacted soils wrapped in plastic from the site and properly disposing of them. The Department has given the operator ample of time to properly remove the impacted soils. Please remove the impacted soils and upon doing so, provide the Department w |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2749379 | 821707 | 2018-07-02 | CSL 402(b) | Environmental Health & Safety | Brine water was released to the ground. | |
2749379 | 821708 | 2018-07-02 | 78.57(a) | Environmental Health & Safety | The operator failed to control and dispose of brine water. | |
2749379 | 821709 | 2018-07-02 | SWMA 301 | Environmental Health & Safety | Operator failed to control and dispose of brine water. | |
2768535 | 826613 | 2018-07-02 | CSL 402(b) | Environmental Health & Safety | Brine water was released to the ground. | |
2768535 | 826614 | 2018-07-02 | 78.57(a) | Environmental Health & Safety | The operator failed to control and dispose of brine water. | |
2768535 | 826615 | 2018-07-02 | SWMA 301 | Environmental Health & Safety | Operator failed to control and dispose of brine water. | |
2784683 | 829839 | 2018-07-02 | CSL 402(b) | Environmental Health & Safety | Brine water was released to the ground. | |
2784683 | 829840 | 2018-07-02 | 78.57(a) | Environmental Health & Safety | The operator failed to control and dispose of brine water. | |
2784683 | 829841 | 2018-07-02 | SWMA 301 | Environmental Health & Safety | Operator failed to control and dispose of brine water. | |
2856846 | 844760 | 2018-07-02 | CSL 402(b) | Environmental Health & Safety | Brine water was released to the ground. | |
2856846 | 844761 | 2018-07-02 | 78.57(a) | Environmental Health & Safety | The operator failed to control and dispose of brine water. | |
2856846 | 844762 | 2018-07-02 | SWMA 301 | Environmental Health & Safety | Operator failed to control and dispose of brine water. |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
821707 | 365364 | NOV - Notice of Violation | |||||
821708 | 365364 | NOV - Notice of Violation | |||||
821709 | 365364 | NOV - Notice of Violation |
For data sources see[7]