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37-027-20122

Well Details

Well ID: 37-027-20122
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Country: United States
State: Pennsylvania
County: Centre
Municipality: Rush Township
Operator Name: CAPITAL OIL & GAS INC
Well Pad ID:
Farm/Lease Name: COP TR 243
License Status: Plugged and Abandoned
Spud Date: 1985-07-03
Permit Date: 1985-05-20
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.902268
Longitude: -78.089907

For data sources see[1][2][3]

Well History

Date Event
1985-05-20 New Permit Application
1985-07-03 Performed Spud Operation
1985-07-11 Drilling Completion
1985-07-15 Perforation
1986-01-01 NEWLY DRILLED
2018-06-28 Begin Plugging
2018-06-29 Finished Plugging
2018-08-17 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1989 EQUITABLE PROD EASTERN STATES EXPLORATION INC 2,200.00 360 0.00 0 0.00 0
1990 EQUITABLE PROD EASTERN STATES EXPLORATION INC 1200.00 360 0.00 0 0.00 0
1991 EQUITABLE PROD EASTERN STATES EXPLORATION INC 434.00 360 0.00 0 0.00 0
1992 EQUITABLE PROD EASTERN STATES EXPLORATION INC 669.00 360 0.00 0 0.00 0
1994 EQUITABLE PROD EASTERN STATES EXPLORATION INC 436.00 365 0.00 0 0.00 0
1995 EQUITABLE PROD EASTERN STATES EXPLORATION INC 1102.00 365 0.00 0 0.00 0
1996 EQUITABLE PROD EASTERN STATES EXPLORATION INC 823 365 0.00 0 0.00 0
1997 EQUITABLE PROD EASTERN STATES EXPLORATION INC 1621 365 0.00 0 0.00 0
1998 EQUITABLE PROD EASTERN STATES EXPLORATION INC 510 365 0.00 0 0.00 0
1999 EQUITABLE PROD EASTERN STATES EXPLORATION INC 231 365 0.00 0 0.00 0
2000 EQUITRANS INC 165 365 0.00 0 0.00 0
2001 EQUITABLE PROD EASTERN STATES EXPLORATION INC 111 365 0.00 0 0.00 0
2003 EQT PROD CO 382 365 0.00 0 0.00 0
2004 EQT PROD CO 293 366 0.00 0 0.00 0
2005 NCL NATURAL RESOURCES LLC 431 365 0.00 0 0.00 0
2006 NCL NATURAL RESOURCES LLC 217.00 365 0.00 0 0.00 0
2007 NCL NATURAL RESOURCES LLC 657.00 365 0.00 0 0.00 0
2008 NCL NATURAL RESOURCES LLC 238.00 365 0.00 0 0.00 0
2009 NCL NATURAL RESOURCES LLC 239.00 349 0.00 0 0.00 0
2010 NCL NATURAL RESOURCES LLC 181.00 365 0.00 0 0.00 0
2011 NCL NATURAL RESOURCES LLC 46.00 365 0.00 0 0.00 0
2012 NCL NATURAL RESOURCES LLC 0.00 0 0.00 0 0.00 0
2013 NCL NATURAL RESOURCES LLC 48.00 365 0.00 0 0.00 0
2014 NCL NATURAL RESOURCES LLC 0.00 0 0.00 0 0.00 0
2015 NCL NATURAL RESOURCES LLC 0.00 0 0.00 0 0.00 0
2016 NCL NATURAL RESOURCES LLC 325.00 365 0.00 0 0.00 0
2017 CAPITAL OIL & GAS INC 0.00 0 0.00 0 0.00 0
2018 CAPITAL OIL & GAS INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
211132 Primary Facility 1987-10-21 Routine/Complete Inspection No Violations Noted E&S OK;BRINE TANK
2747242 Primary Facility 2018-06-29 Plugging(Includes Plugged/Mined Through) No Violations Noted Nick's Well Plugging are on location for plug and abandonment. The rig is in the middle of pulling 38 jts of 4 1/2" after setting final cement plug across surface casing shoe (used retrieved 4 1/2" production casing as workstring). No gas was detected inside the 4 1/2" with an Altair 5x gas meter. Annulus is isolated and lined out to a tank from casinghead, though the annulus now has communication with 4 1/2" (no gas). There was standing water outside of surface casing with no bubbling observed. No obvious issues were observed.
2753734 Primary Facility 2018-07-19 Plugging(Includes Plugged/Mined Through) No Violations Noted Nick's Well Plugging are off location following final plug and abandonment. The plugged well has been cut and buried and a 2" vent pipe has been installed on the well extending above ground level. There were no open holes, discharges, venting, or any other obvious issues visible. No combustible gas was detected at the vent with an Altair 5x gas meter.

For data sources see[6]

References