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37-021-21041

Well Details

Well ID: 37-021-21041
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Country: United States
State: Pennsylvania
County: Cambria
Municipality: Chest Township
Operator Name: DORSO LP
Well Pad ID:
Farm/Lease Name: JACOB & HENRY LEIDEN HEIRS 16
License Status: ACTIVE
Spud Date:
Permit Date: 2007-03-15
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.710309
Longitude: -78.633264

For data sources see[1][2][3]

Well History

Date Event
2006-06-21 Perforation
2007-03-15 New Permit Application
2007-06-11 Performed Spud Operation
2007-06-14 Drilling Completion
2007-09-06 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2007 DORSO LP 2765.00 365 0.00 0 0.00 0
2008 DORSO LP 9070.00 365 0.00 0 0.00 0
2009 DORSO LP 6396.00 365 0.00 0 0.00 0
2010 DORSO LP 4,886.00 365 0.00 0 0.00 0
2011 DORSO LP 4,570.00 365 0.00 0 0.00 0
2012 DORSO LP 4,316.00 365 0.00 0 0.00 0
2013 DORSO LP 3,745.00 365 0.00 0 0.00 0
2014 DORSO LP 1,151.00 365 0.00 0 0.00 0
2015 DORSO LP 3,231.00 365 0.00 0 0.00 0
2016 DORSO LP 1,896.00 304 0.00 0 0.00 0
2017 DORSO LP 1,395.00 273 0.00 0 0.00 0
2018 DORSO LP 2,518.00 365 0.00 0 0.00 0
2019 DORSO LP 1,862.00 365 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1885806 Primary Facility 2010-05-19 Routine/Complete Inspection No Violations Noted According to records, well completed on 6/14/07 to a depth of 3,676 ft. Active permit since 3/17/07. Well head completed with 8¿ pipe reduced to 4¿ and reduced to 2¿ production line with 5 shut off valves. Production equipment consisted of separator (180 psi), data logger (150/25 psi), 100 bbl brine tank (< 20 bbl fluid) and rabbit float. No IW issues during inspection surrounding the production well. Farm name on meter box. E&S issues at the site. Site has not been restored. Took pictures of the site. Request WQ personnel perform inspection of the site. Slight gas odor around the separator. Dent located in the poly brine tank. Slight leak appeared around flange of inlet pipe to brine tank. Talked to Chad Wagner (Dorso) field supervisor about issues.
2411966 Primary Facility 2015-09-30 Routine/Complete Inspection No Violations Noted At time of inspection well tag present, legible and affixed in a permanent manner.
2626002 Primary Facility 2017-08-15 Routine/Complete Inspection No Violations Noted well was in production. No issues with well.

For data sources see[6]

References