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37-021-21036

Well Details

Well ID: 37-021-21036
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Country: United States
State: Pennsylvania
County: Cambria
Municipality: Allegheny Township
Operator Name: ADMIRAL BAY USA INC
Well Pad ID:
Farm/Lease Name: WEILAND 1
License Status: PLUGGED & ABANDONED
Spud Date: 2008-02-24
Permit Date: 2007-02-15
Well Type: COALBED METHANE
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.546572
Longitude: -78.662055

For data sources see[1][2][3]

Well History

Date Event
2007-02-15 New Permit Application
2008-01-09 Permit Renewal Application
2008-02-21 Performed Spud Operation
2008-02-27 Drilling Completion
2008-07-24 Perforation
2008-09-26 NEWLY DRILLED
2012-11-14 Drilling Completion
2013-02-28 FULLY PLUGGED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2007 ADMIRAL BAY USA INC 0.00 0 0.00 0 0.00 0
2010 ADMIRAL BAY USA INC 0.00 0 0.00 0 0 365
2012 ADMIRAL BAY USA INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1817896 Primary Facility 2009-08-03 Routine/Complete Inspection No Violations Noted Drilling was completed 2/27/2008. The well site has been restored and is well vegetated. Well is equipped with a pump jack, which is not in operation at the time of the inspection. Brine tank is in sound condition. No signs of erosion and sedimentation on the well site and access road.
1846775 Primary Facility 2009-12-01 Routine/Complete Inspection No Violations Noted According to records, permit was granted 2/15/07. Well was completed on 2/5/09 to a depth of 1142 ft. WRAC report was submitted and approved on 3/21/08. Well tag present but was disconnected from wellhead and needs reconnected. Well head consisted of 8¿ pipe reduced to 4¿ to 2¿ shut off valve. Well head consisted of 8¿ pipe reduced to 4¿ to 2¿ production pipe with 5 shut off valves (in the off position). Production equipment consisted of jack pump connected to well head, propane tank, data logger and two 100 bbl poly brine tanks. No signs of gas leakage around well head. At the time of inspection, no IW or E&S issues at the site.
2155689 Primary Facility 2013-04-04 Routine/Complete Inspection No Violations Noted Well plugged on 11/14/2012. Monument buried. Located in ag field. Shared access road in good condition. No accelerated erosion or sedimentation issues observed in relation to well site or access road.
2195182 Primary Facility 2013-07-29 Site Restoration No Violations Noted Well plugged on 11/14/2012. Monument buried. Located in ag field. Shared access road in good condition. No accelerated erosion or sedimentation issues observed in relation to well site or access road.
2204190 Primary Facility 2013-09-05 Bond Release No Violations Noted Bond release inspection. Well plugged on 11/14/2012. Buried monument. Access road stable. No accelerated erosion or sedimentation issues observed in relation to well site or access road.

For data sources see[6]

References