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37-015-22731

Well Details

Well ID: 37-015-22731
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Country: United States
State: Pennsylvania
County: Bradford
Municipality: Wilmot Township
Operator Name: CHIEF OIL & GAS LLC
Well Pad ID: 148788
Farm/Lease Name: LUCARINO UNIT 2H
License Status:
Spud Date:
Permit Date: 2013-10-09
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.559592
Longitude: -76.275053

For data sources see[1][2][3]

Well History

Date Event
2013-10-09 New Permit Application
2013-10-27 Performed Spud Operation
2014-01-10 Perforation
2014-05-20 DEVIATED

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2014-01-18 2014-01-27 8,478 8,861,120

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 BA-40L Halliburton Buffering Agent Potassium Carbonate 584-08-7 60 0.001 0
FR-66 Halliburton Friction Reducer Hydrotreated Light Petroleum Distillate 64742-47-8 30 0.03 0
Water Provided by Customer Base Fluid Fresh Water 0000-00-0 100 99.88 0
Bactron K-139 Champion Technologies Biocide Glutaraldehyde 111-30-8 5 0.002 0
Quaternary ammonium compounds,
benzyl-C-12-16 alkyldimethyl, chlorides
68424-85-1 10 0.004 0
Ethanol 64-17-5 5 0.002 0
Hydrochloric Acid 10-30% Halliburton Acid Hydrochloric Acid 7647-01-0 30 0.1 0
Gyptron T-390 Champion Technologies Scale Inhibitor Methanol 67-56-1 10 0.001 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2013 CHIEF OIL & GAS LLC 0.00 0 0.00 0 0.00 0
2014 CHIEF OIL & GAS LLC 3,057,369.00 323 0.00 0 0.00 0
2015 CHIEF OIL & GAS LLC 2,133,816.78 315 0.00 0 0.00 0
2016 CHIEF OIL & GAS LLC 1,482,256.24 324 0.00 0 0.00 0
2017 CHIEF OIL & GAS LLC 992,545.40 348 0.00 0 0.00 0
2018 CHIEF OIL & GAS LLC 917,067.18 358 0.00 0 0.00 0
2019 CHIEF OIL & GAS LLC 1,053,321.47 365 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2013 CHIEF OIL & GAS LLC Drilling Fluid Waste 330.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR119
2013 CHIEF OIL & GAS LLC Drill Cuttings 1,546.62 Tons LANDFILL 100933
2013 CHIEF OIL & GAS LLC Drilling Fluid Waste 102.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123SW018
2014 CHIEF OIL & GAS LLC Drilling Fluid Waste 279.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123SW018
2014 CHIEF OIL & GAS LLC Drill Cuttings 91.40 Tons LANDFILL 100933
2014 CHIEF OIL & GAS LLC Fracing Fluid Waste 6,524.00 Bbl REUSE OTHER THAN ROAD SPREADING
2014 CHIEF OIL & GAS LLC Fracturing Fluid Waste 53.83 Tons LANDFILL 301358
2014 CHIEF OIL & GAS LLC Produced Fluid 3,713.77 Bbl REUSE OTHER THAN ROAD SPREADING
2014 CHIEF OIL & GAS LLC Fracing Fluid Waste 880.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC018
2014 CHIEF OIL & GAS LLC Drill Cuttings 510.79 Tons LANDFILL 301358
2015 CHIEF OIL & GAS LLC Produced Fluid 913.01 Bbl REUSE OTHER THAN ROAD SPREADING
2016 CHIEF OIL & GAS LLC Produced Fluid 643.39 Bbl REUSE OTHER THAN ROAD SPREADING
2017 CHIEF OIL & GAS LLC Produced Fluid 61.68 Bbl STORAGE PENDING DISPOSAL OR REUSE
2017 CHIEF OIL & GAS LLC Produced Fluid 115.35 Bbl REUSE (AT WELL PAD)
2018 CHIEF OIL & GAS LLC Produced Fluid 634.10 Bbl REUSE (AT WELL PAD)
2019 CHIEF OIL & GAS LLC Produced Fluid 451.43 Bbl REUSE (AT WELL PAD)

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2218189 Primary Facility 2013-10-28 Drilling/Alteration Pending Ziegenfuss, Comp Man - Tony Tripp who is not here, talked to Armando
2220182 Primary Facility 2013-10-28 Routine/Complete Inspection No Violations Noted
2224764 Primary Facility 2013-11-20 Routine/Complete Inspection No Violations Noted
2229378 Primary Facility 2013-12-12 Drilling/Alteration No Violations Noted Sidewinder 58, Comp Man - Bill Del Cambre
2273144 Primary Facility 2014-05-20 Routine/Complete Inspection No Violations Noted Arrived 15:00. Workers painting well head. Groups of yellow baker tanks were stationed on the S and W sides of the pad and in the NE corner. Small pieces of foam berm material were scattered around the pad and there were small pieces of felt in many locations. On the south side there was a large pile of frac sand. Most of the puddles on location gave field conductivity readings > 3 mS/cm. A 15' x 6' puddle in front of the sand pile gave field conductivity readings > 8mS/cm (sample 2371 381). Small, (~2' diameter) fuel stains were also found on E &W sides. The result of this inspection for the 3H well (015-22732) is pending the sample results.
2372692 Primary Facility 2015-05-20 Routine/Complete Inspection No Violations Noted Arrived @ 13:40. Sunny, cold, cloudy. There were three wells, all in production, on the pad. There was some pressure on the 3H 9-5/8” x 5-1/2” annulus. This blew down in a few seconds.
2387375 Primary Facility 2015-07-09 Routine/Complete Inspection No Violations Noted Arrived @ 15:00 with Compliance Specialist Tony Liguori. Weather: breezy, sunny. There were three wells on this pad and all three were in production. There was some pressure on the 3H 9-5/8” x 5-1/2” annulus. This did not significantly inflate a glove after 10 minutes. Annular vents were plumbed into poly tanks.
2467771 Primary Facility 2016-03-24 Routine/Complete Inspection No Violations Noted The well pad has been partially restored. The surface has been de-compacted and revegetated. No re-grading was evident.

Overall vegetation on site is approximately 70%, though some bare and rocky areas are present. No evidence of accelerated erosion or sedimentation was observed.

No violations were cited during this inspection.

2519142 Primary Facility 2016-09-15 Administrative/File Review No Violations Noted Administrative inspection conducted in repsonse to well site restoration reports (WSRR) filed by Chief on 09/09/2016. The notice of termination for this site was previously approved by the Department on 07/22/2016 (Inspection No. 2506949).

Interim restoration has been implemented on the well pad. A significant portion of the pad surface has been decompacted and vegetated. A total of 5,160 tons of drill cuttings, 711 barrels of drilling fluid, and 21,914 barrels fracing fluid are reported to have been disposed of at appropriate waste disposal facilities.

The well site restoration reports are acknowledged.

2592793 Primary Facility 2017-05-09 Routine/Complete Inspection No Violations Noted Three wells in production phase. Three separators within containment. One suction engine on site. Site stable. No violations noted.
2679614 Primary Facility 2018-01-08 Routine/Complete Inspection No Violations Noted Three wells in production phase. Three each sand and water separators. No leaks detected from production equipment. Suction engine in use on location. No violations noted.
2703846 Primary Facility 2018-03-06 Routine/Complete Inspection No Violations Noted Arrived at 11:49. Weather: sunny. There are three wells capable of production but temporarily shut-in on this location At the time of my inspection crew we're working on the on-site compressor and performing maintenance on the GPUs.
2814347 Primary Facility 2018-12-12 Routine/Complete Inspection No Violations Noted Arrived onsite for a routine inspection at 09:57; the weather was ~30°F and calm. There was a light dusting of snow on the pad and surrounding area.

There were 3 tagged Marcellus wells staged for production. The 3 well cellars were filled with gravel. The 2H well tag shows Stevens Twp., however, the permit sign near the mailbox shows Wilmot Twp. (Photos #2, 3).

There were 3 GPUs, 4 produced water tanks, and a compressor onsite and in secondary containment. There was also a freshwater injection tank plumbed to the wells.

The pad area was reduced and the site was greater than 70% vegetative cover. Both the cut and fill side of the pad had steeper sections that were stabilized with rock. The site appeared stable; no E&S issues were noted.

It is recommended that the tags for the 2H well be corrected as needed.

No violations were observed during the inspection.

For data sources see[8]

References