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37-005-30413

Well Details

Well ID: 37-005-30413
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: North Buffalo Township
Operator Name: MDS ENERGY DEV LLC
Well Pad ID:
Farm/Lease Name: DOUGLAS A FLANDERS ETUX 1-.7
License Status:
Spud Date:
Permit Date: 2009-07-28
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.802741
Longitude: -79.533118

For data sources see[1][2][3]

Well History

Date Event
2009-07-28 New Permit Application
2010-07-06 Performed Spud Operation
2010-07-10 Drilling Completion
2010-10-13 Perforation
2011-03-25 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 MDS ENERGY LTD 0.00 0 0.00 0 0.00 0
2011 MDS ENERGY LTD 6,208.00 365 0.00 0 0.00 0
2012 MDS ENERGY LTD 6,000.00 366 0.00 0 0.00 0
2013 MDS ENERGY LTD 3,651.00 362 0.00 0 0.00 0
2014 MDS ENERGY LTD 2,807.00 303 0.00 0 0.00 0
2015 MDS ENERGY DEV LLC 2,460.00 364 0.00 0 0.00 0
2016 MDS ENERGY DEV LLC 1,283.00 366 0.00 0 0.00 0
2017 MDS ENERGY DEV LLC 2,094.00 364 0.00 0 0.00 0
2018 MDS ENERGY DEV LLC 484.00 358 0.00 0 0.00 0
2019 MDS ENERGY DEV LLC 383.00 357 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 MDS ENERGY LTD Drilling Fluid Waste 240.00 Bbl REUSE OTHER THAN ROAD SPREADING
2011 MDS ENERGY LTD Produced Fluid 100.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472
2011 MDS ENERGY LTD Produced Fluid 151.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1922211 Primary Facility 2010-10-19 Routine/Complete Inspection No Violations Noted Well shut in on 2¿ tubing. Rods installed. Pump jack not yet installed. 7¿ x 2¿ annulus closed. Evidence of slight gas expression at 7¿ x 9 5/8¿ annulus. Pit lined and freeboard maintained at time of inspection. Discussed E/S controls issues (downgrade silt fence) with operator rep Randy Morris. Referred to WQS J. Shultz for follow up. Inspection conducted w/OGI D. Catalano.
1929375 Primary Facility 2010-10-22 Routine/Complete Inspection No Violations Noted Well is drilled, but not equipped for production. Crew is on-site / installing the pipe for the brine tank. Site ID sign and E&S plan located. There are no signs of erosion or sedimentation on the well site or access road.
1929376 Primary Facility 2010-11-22 Complaint Inspection No Violations Noted Inspection performed as the result of a complaint.

For data sources see[7]

References