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Well ID: 37-005-30334 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Armstrong | |
Municipality: Kiskiminetas Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: CHARLES RIGGLE 3 | |
License Status: | |
Spud Date: | |
Permit Date: 2009-04-24 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.620012 | |
Longitude: -79.450894 |
Date | Event |
---|---|
2009-04-24 | New Permit Application |
2010-03-19 | Performed Spud Operation |
2010-03-25 | Drilling Completion |
2010-03-29 | Perforation |
2010-12-02 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2009 | CONSOL GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | CONSOL GAS CO | 12,549.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | CONSOL GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CNX GAS CO LLC | 9,048.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | CNX GAS CO LLC | 6,985.69 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | CNX GAS CO LLC | 7,013.13 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | CNX GAS CO LLC | 5,946.84 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | CNX GAS CO LLC | 3,816.44 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | CNX GAS CO LLC | 1,501.83 | 304 | 0.00 | 0 | 0.00 | 0 |
2018 | CNX GAS CO LLC | 1,149.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | ALLIANCE PETRO CO LLC | 1,817.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2010 | CONSOL GAS CO | Fracing Fluid Waste | 400.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2010 | CONSOL GAS CO | Produced Fluid | 89.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2010 | CONSOL GAS CO | Fracing Fluid Waste | 480.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095443 |
2011 | CNX GAS CO LLC | Produced Fluid | 89.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2012 | CNX GAS CO LLC | Produced Fluid | 66.17 Bbl | INJECTION DISPOSAL WELL | 34-013-20609 |
2014 | CNX GAS CO LLC | Produced Fluid | 30.09 Bbl | INJECTION DISPOSAL WELL | 34-013-20609 |
2019 | ALLIANCE PETRO CO LLC | Produced Fluid | 77.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1872333 | Primary Facility | 2010-03-25 | Routine/Complete Inspection | No Violations Noted | Drill rig located onsite and drilling was ongoing at the time of the inspection. Observed no accelerated erosion & sedimentation on the access road or well-site. Below grade pit located onsite and it had more than the required two feet of freeboard. When moving the drill rig off-site the operator should have a broom truck onsite to deal with any mud generated and deposited on SR 2033. In addition the operator should regrade and rerock the access road prior to any well stimulation is undertaken |
2068796 | Primary Facility | 2012-05-17 | Site Restoration | No Violations Noted | Drilling was completed on 03/25/10. Well appeared to be equipped for production. Brine tank located onsite and it appeared to be in sound condition. Site had been properly restored. Vegetation met the 70% uniform coverage criteria. There was no observed accelerated erosion or sedimentation observed in relation to the access road or well-site. |
For data sources see[7]