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37-003-22420

Well Details

Well ID: 37-003-22420
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Country: United States
State: Pennsylvania
County: Allegheny
Municipality: Moon Township
Operator Name: UNKNOWN OPR
Well Pad ID:
Farm/Lease Name:
License Status:
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Undetermined
Conservation: No
Latitude: 40.5285
Longitude: -80.226694

For data sources see[1][2][3]



Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2524775 Primary Facility 2016-09-13 Routine/Complete Inspection No Adverse Event or Action Reported Wellhead is 6" casing swaged to 3 1/2" reduced to 2 2/8", topped w/ valve and old gas light fixture. Well is leaking a very small amount of gas. Wellhead is 25 feet from powerlines, 25 feet from driveway and 175 feet from nearest house in flat wooded area of lawn.
2619052 Primary Facility 2017-07-26 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to inspect well after receiving a call from a representative of Civil Environmental Consultants. Excavation is scheduled to begin to develop the property. The well and area surrounding it will not be disturbed. Wellhead is intact and unchanged from 9/13/16 inspection. No gas leaks detected, although it was windy.
2689844 Primary Facility 2018-02-01 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to check status of abandoned well. Unable to safely get back to wellsite due to high level of excavation and construction activity going on at property.
2705356 Primary Facility 2018-03-14 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to inspect well during surrounding excavation and construction. Well remains undamaged and intact. Contractor has poured concrete pad around base of wellhead. Well is ringed by construction trailers and large rock. Talked to representatives from Continental about well.
2773304 Primary Facility 2018-08-22 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to inspect well during surrounding excavation and construction. Well remains undamaged and intact.
2781896 Primary Facility 2018-10-01 Plugging(Includes Plugged/Mined Through) No Violations Noted When the well was opened up there was 6" casing 3' down in the well. 2" tubing is being run in the well to set a bottom plug to shut off the gas. The plan is to then log and pull the 6" casing.
2781986 Primary Facility 2018-10-01 Plugging(Includes Plugged/Mined Through) No Viols - Permanently Shut Down Nick's Well Service rigged up on well and tagged bottom at ~2200'. TIH with work string to 1190' and shut down. Remainder of tubing will be run tomorrow AM. Plan is to spot bottom hole plug in morning, then log hole in afternoon.
2782720 Primary Facility 2018-10-02 Plugging(Includes Plugged/Mined Through) No Viols - Permanently Shut Down Appalachian Well Services logged hole and tagged TD at 2204'. The bottom hole plug that Nicks Well Plugging pumped yesterday was all taken downhole by formation (?) as there was no trace of cement. Discussed log results. Appears none of the 1796' of 6 5/8" casing is free and will need perforations to surface.
2782800 Primary Facility 2018-10-02 Plugging(Includes Plugged/Mined Through) No Viols - Permanently Shut Down Appalachian Well Surveys are perforating the 6 5/8" casing, 10 shots per 100' in 3-4-3 groupings, starting at 1700'.
2783896 Primary Facility 2018-10-03 Plugging(Includes Plugged/Mined Through) No Viols - Permanently Shut Down Nick's Well Plugging pumped two 700' (calculated) plugs, then SD. Will tag TOC and resume plugging tomorrow AM.
2784377 Primary Facility 2018-10-04 Plugging(Includes Plugged/Mined Through) No Viols - Permanently Shut Down Nick's Well Plugging tagged yesterday's plug TOC at 865', pumped remaining plug to surface. Good returns with circulation up backside. Rigging down.

For data sources see[4]

References