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Well ID: 37-003-22384 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Allegheny | |
Municipality: South Fayette Township | |
Operator Name: UNKNOWN OPR | |
Well Pad ID: | |
Farm/Lease Name: | |
License Status: | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Undetermined | |
Conservation: No | |
Latitude: 40.360556 | |
Longitude: -80.215528 |
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2598494 | Primary Facility | 2015-12-17 | Routine/Complete Inspection | No Viols - Permanently Shut Down | Visited site w/ (RETTEW) representative as part of the Southern Beltway Project. Wellhead is 10" conductor, 6" surface casing and 5" production casing. The 5" casing is open to an unknown depth, where it is filled with water and gassing (100% LEL- Altair). Other pipes still in ground around wellhead are what remains from base of metal walking beam and other structures. Well is along old access road in slightly sloped wooded and brushed area ~ 25 feet from a small stream. |
2598495 | Primary Facility | 2017-04-14 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost rig is @ 24 feet, cleaning out wood. |
2598497 | Primary Facility | 2017-04-17 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost rig is @123 feet, drilled out wooden plug w/ some gas behind. Gurgles loudly. |
2598501 | Primary Facility | 2017-04-24 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost rig is milling @ 146 feet. They lost circulation @ surface, so they reset the conductor and solved the problem. |
2598506 | Primary Facility | 2017-04-25 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost milling hard obstruction w/ flat-bottom mill @ 164 feet. Earlier trip in w/overshot did not yield anything. |
2598509 | Primary Facility | 2017-04-27 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost rig is cleaning wood out of hole @ 271 feet, making 3-4 feet/hr. |
2598513 | Primary Facility | 2017-05-08 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost ran camera to try to evaluate problem areas in well. Work string may be on outside of casing, drilling new hole. Set down @ 151 feet & 162 feet (well cleaned out to 250 feet). Tried to blow well dry, but fluid level stayed @~130 feet. |
2598520 | Primary Facility | 2017-05-09 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost appears to be back in wellbore again after possibly sidetracking, cleaning out @ 526 feet. Cannot keep fluid circulation, so will try drying hole & switch to air. |
2598525 | Primary Facility | 2017-05-16 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost rig is off well and well is plugged from ~650 feet to surface. (*Attainable bottom was called @~700 feet, due to rapidly deteriorating hole conditions. TIMCO logged and perforated the casing every 50 feet prior to cementing.) |
For data sources see[4]